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34-167-20025

Well Details

Well ID: 34-167-20025
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Country: United States
State: Ohio
County: Washington
Municipality: Liberty Township
Operator Name: GAS ENTERPRISE COMPANY INC
Well Pad ID:
Farm/Lease Name: MARION EPIER HRS
License Status: Producing
License Date:
Spud Date: 1937-06-05
Spud Drilling Contractor:
Final Drill Date: 1937-06-15
Well Total Depth: 1122.00 ft
Configuration: Vertical
Latitude: 39.530000
Longitude: -81.300000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1937-06-05 OWNERSHIP CHANGED AS PER MEETING WITH JIM, CINDY VAN DYKE AND MIKE MCCORMAC ON DECEMBER 2, 2005.
Completed 1937-06-15 OWNERSHIP CHANGED AS PER MEETING WITH JIM, CINDY VAN DYKE AND MIKE MCCORMAC ON DECEMBER 2, 2005.
Reached Total Depth 1937-06-15 OWNERSHIP CHANGED AS PER MEETING WITH JIM, CINDY VAN DYKE AND MIKE MCCORMAC ON DECEMBER 2, 2005.
Record Last Modified 2013-10-03 OWNERSHIP CHANGED AS PER MEETING WITH JIM, CINDY VAN DYKE AND MIKE MCCORMAC ON DECEMBER 2, 2005.

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1989 TMR OPERATING CO INC 1319.00 0.00 300
2003 GAS ENTERPRISE COMPANY INC 98.00 0.00 365
2004 GAS ENTERPRISE COMPANY INC 102.00 0.00 365
2005 GAS ENTERPRISE COMPANY INC 115.00 0.00 365
2006 GAS ENTERPRISE COMPANY INC 13.00 0.00 365
2007 GAS ENTERPRISE COMPANY INC 166.00 0.00 365
2008 GAS ENTERPRISE COMPANY INC 192.00 0.00 365
2009 GAS ENTERPRISE COMPANY INC 205.00 0.00 365
2010 GAS ENTERPRISE COMPANY INC 106.00 0.00 365
2011 GAS ENTERPRISE COMPANY INC 13.00 13.00 365
2012 GAS ENTERPRISE COMPANY INC 28.00 0.00 366
2013 GAS ENTERPRISE COMPANY INC 55.00 0.00 365
2014 GAS ENTERPRISE COMPANY INC 45.00 51.00 365
2015 GAS ENTERPRISE COMPANY INC 83.00 5.00 365
2016 GAS ENTERPRISE COMPANY INC 86.00 0.00 365
2017 GAS ENTERPRISE COMPANY INC 75.00 0.00 365
2018 GAS ENTERPRISE COMPANY INC 30.00 0.00 365

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1989 TMR OPERATING CO INC Brine 0 300
2003 GAS ENTERPRISE COMPANY INC Brine 0 365
2004 GAS ENTERPRISE COMPANY INC Brine 0 365
2005 GAS ENTERPRISE COMPANY INC Brine 365
2006 GAS ENTERPRISE COMPANY INC Brine 0 365
2007 GAS ENTERPRISE COMPANY INC Brine 0 365
2008 GAS ENTERPRISE COMPANY INC Brine 0 365
2009 GAS ENTERPRISE COMPANY INC Brine 0 365
2010 GAS ENTERPRISE COMPANY INC Brine 0 365
2011 GAS ENTERPRISE COMPANY INC Brine 0 365
2012 GAS ENTERPRISE COMPANY INC Brine 0 366
2013 GAS ENTERPRISE COMPANY INC Brine 0 365
2014 GAS ENTERPRISE COMPANY INC Brine 0 365
2015 GAS ENTERPRISE COMPANY INC Brine 0 365
2016 GAS ENTERPRISE COMPANY INC Brine 0 365
2017 GAS ENTERPRISE COMPANY INC Brine 0 365
2018 GAS ENTERPRISE COMPANY INC Brine 0 365

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1330113342 2012-02-22 Production Wells No Violations My inspection this day is routine. I found well capable of producing with a pumping unit, valves open at well, good identification at well. No tank found, no meter found.
1599623968 2012-11-27 Administrative Inspection No Violations Jim Williams called to report he has this well back in production. Since I looked at well, it had gone down, they pulled equipment and found holes in the 5.5 casing (down to 920). Ran 3.5 casing on a packer set at 903, then rods and tubing back in and put to pump. Also found leaks in the gas line and repaired them.

For data sources see[7]

References