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Well ID: 34-119-22406 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Harrison Township | |
Operator Name: MAJOR PRODUCING LLC | |
Well Pad ID: | |
Farm/Lease Name: WM STUTES & HEIRS | |
License Status: Producing | |
License Date: 1970-11-11 | |
Spud Date: 1970-11-09 | |
Spud Drilling Contractor: | |
Final Drill Date: 1971-01-16 | |
Well Total Depth: 1254.00 ft | |
Configuration: Vertical | |
Latitude: 39.800000 | |
Longitude: -81.930000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1970-11-05 | 3108 MAJOR PRODUCING CORP GeoDate 11/5/70 |
Original Spud | 1970-11-09 | |
Completed | 1971-01-16 | |
Reached Total Depth | 1971-01-16 | |
CO | 1994-12-29 | 1868 DUSTY DRILL & PRO CORP GeoDate 11/5/70 |
Change of Owner | 2003-11-05 | Operator changed from 1868, DUSTY DRILL & PRO CORP to 2867, DNL OIL CORP |
Change of Owner | 2012-08-02 | Operator changed from 2867, DNL OIL CORP to 9019, ALTIER N L JR |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | S/W 250# & 30 QTS. |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | DUSTY DRILLING & PRODUCING COR | 0.00 | 135.00 | 0 |
1985 | DUSTY DRILLING & PRODUCING COR | 0.00 | 150.00 | 295 |
1986 | DUSTY DRILLING & PRODUCING COR | 0.00 | 130.00 | 274 |
1988 | MAJOR PRODUCING CORP | 0.00 | 113.00 | 365 |
1991 | MAJOR PRODUCING CORP | 0.00 | 107.00 | 180 |
1992 | MAJOR PRODUCING CORP | 0.00 | 63.00 | 150 |
1993 | MAJOR PRODUCING CORP | 0.00 | 138.00 | 150 |
1994 | DUSTY DRILLING & PRODUCING COR | 0.00 | 29.00 | 365 |
1997 | DUSTY DRILLING & PRODUCING COR | 0.00 | 13.00 | 365 |
1998 | DUSTY DRILLING & PRODUCING COR | 0.00 | 136.00 | 365 |
2001 | DUSTY DRILLING & PRODUCING COR | 0.00 | 0.00 | 0 |
2002 | DUSTY DRILLING & PRODUCING COR | 0.00 | 37.00 | 83 |
2003 | DUSTY DRILLING & PRODUCING COR | 0.00 | 16.00 | 270 |
2004 | DNL OIL CORP | 0.00 | 7.00 | 50 |
2005 | DNL OIL CORP | 0.00 | 0.00 | 0 |
2006 | DNL OIL CORP | 0.00 | 0.00 | 40 |
2007 | DNL OIL CORP | 0.00 | 58.00 | 40 |
2008 | DNL OIL CORP | 0.00 | 45.00 | 40 |
2009 | DNL OIL CORP | 0.00 | 67.00 | 55 |
2010 | DNL OIL CORP | 0.00 | 63.00 | 115 |
2011 | DNL OIL CORP | 0.00 | 105.00 | 365 |
2012 | DNL OIL CORP | 0.00 | 0.00 | 243 |
2013 | ALTIER N L JR | 0.00 | 147.00 | 365 |
2014 | ALTIER N L JR | 0.00 | 108.00 | 365 |
2015 | ALTIER N L JR | 0.00 | 96.00 | 335 |
2016 | ALTIER N L JR | 0.00 | 87.00 | 365 |
2017 | ALTIER N L JR | 0.00 | 104.00 | 343 |
2018 | ALTIER N L JR | 0.00 | 128.00 | 315 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | DUSTY DRILLING & PRODUCING COR | Brine | 0 | 0 |
1985 | DUSTY DRILLING & PRODUCING COR | Brine | 73 | 295 |
1986 | DUSTY DRILLING & PRODUCING COR | Brine | 63 | 274 |
1988 | MAJOR PRODUCING CORP | Brine | 70 | 365 |
1991 | MAJOR PRODUCING CORP | Brine | 0 | 180 |
1992 | MAJOR PRODUCING CORP | Brine | 69 | 150 |
1993 | MAJOR PRODUCING CORP | Brine | 70 | 150 |
1994 | DUSTY DRILLING & PRODUCING COR | Brine | 68 | 365 |
1997 | DUSTY DRILLING & PRODUCING COR | Brine | 38 | 365 |
1998 | DUSTY DRILLING & PRODUCING COR | Brine | 22 | 365 |
2001 | DUSTY DRILLING & PRODUCING COR | Brine | 0 | 0 |
2002 | DUSTY DRILLING & PRODUCING COR | Brine | 5 | 83 |
2003 | DUSTY DRILLING & PRODUCING COR | Brine | 25 | 270 |
2004 | DNL OIL CORP | Brine | 15 | 50 |
2005 | DNL OIL CORP | Brine | 0 | 0 |
2006 | DNL OIL CORP | Brine | 0 | 40 |
2007 | DNL OIL CORP | Brine | 15 | 40 |
2008 | DNL OIL CORP | Brine | 20 | 40 |
2009 | DNL OIL CORP | Brine | 27 | 55 |
2010 | DNL OIL CORP | Brine | 47 | 115 |
2011 | DNL OIL CORP | Brine | 27 | 365 |
2012 | DNL OIL CORP | Brine | 36 | 243 |
2013 | ALTIER N L JR | Brine | 57 | 365 |
2014 | ALTIER N L JR | Brine | 23 | 365 |
2015 | ALTIER N L JR | Brine | 15 | 335 |
2016 | ALTIER N L JR | Brine | 38 | 365 |
2017 | ALTIER N L JR | Brine | 34 | 343 |
2018 | ALTIER N L JR | Brine | 13 | 315 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-118365431 | 2015-3-14 0:00: | AM | No Violations | |
-1723884124 | 2015-3-17 0:00: | PW | No Violations | |
-1849353176 | 2015-3-13 0:00: | PW | No Violations | 2.50 |
0118365431 | 2015-03-14 | Administrative Inspection | No Violations | Dan Jones called on the well 119-22406 and he had cleaned up the oil and the debris that was making an issue at the well. The packing is being brought out to repair the pumping unit. |
1723884124 | 2015-03-17 | Production Wells | No Violations | I went in to inspect site as a follow up to Oil incident. The clean up was not satisfactory. I called Dusty Altier and he will be out in the morning of 3-18-15 with peat absorbent and absorbent pads. They will remove all saturated pads. I will meet them in the morning. |
1849353176 | 2015-03-13 | Production Wells | No Violations | I was talking to a landowner named Harold Kinney on a well that was pumping crude all over the ground when the pump would cycle. He gave the name of the landowner which was his nephew. His name was Tim Kinney and he address was at 1280 Virgina Ridge road. I called Tim and stated I would down to look at the situation. I entered the property and Tim was not there so The 10year old son and I went down over the hill to look at the site. I found some crude on the ground from the well head and some puddles. There was about 6-8 gallon of crude in total. We climbed back out of the hollow and pulled up the owner on the well. Dusty Alteir is the owner. He would have the pumper call me. The pumper called back 740-605-6378. His name is Dan Jones. He stated that the packing blew out of the stuffing box. He shut the well in. He would be down to clean up the oil in the morning of 3-14-15. |
2034224242 | 2015-03-18 | Production Wells | No Violations | I met with Dan Jones and Help on site. They were laying absorbent pads down and spreading out absorbant peat. The oil was still being cleaned up. They ran out and will have to go to yard and lay down more absorbant peat. |
For data sources see[8]