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34-139-20646

Well Details

Well ID: 34-139-20646
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Country: United States
State: Ohio
County: Richland
Municipality: Springfield Township
Operator Name: HOUGHTON INVESTMENTS LLC
Well Pad ID:
Farm/Lease Name: O'HAIL J & P {SWIW #2}
License Status: Final Restoration
License Date: 2009-11-30
Spud Date: 1989-04-11
Spud Drilling Contractor:
Final Drill Date: 1989-04-24
Well Total Depth: 1588.00 ft
Configuration: Vertical
Latitude: 40.750000
Longitude: -82.680000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1989-02-09 3243 OHIO PRODUCTION CORP GeoDate 2/9/89
Oil and Gas 1989-02-09 Issued Date 2/9/89 Expired Date 2/9/90 Acres 0010000 Tool Type RTAF Proposed Formation LOCKPORT Proposed Depth 01588 Proposed Drill Depth 01588
Original Spud 1989-04-11 RBDMS Rec
Completed 1989-04-24 RBDMS Rec
Reached Total Depth 1989-04-24 RBDMS Rec
CO 1996-08-27 236 POLING R C CO INC GeoDate 2/9/89
Change of Owner 1999-10-04 Operator changed from 236, POLING R C CO INC to 6227, HOUGHTON INVESTMENTS, L.L.C.
APP 2000-07-07 Proposed Formations:LOCKPORT DOLOMITE, Issued Date:7/7/00, Expired Date:7/7/01 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:SWD, Proposed Well Class:SWIW
APP 2000-07-28 Proposed Formations:LOCKPORT DOLOMITE, Issued Date:07/28/2000, Expired Date:07/28/2001 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:SWD, Proposed Well Class:SWIW
Correction to Well 2000-07-28 NEEDED TO RERUN PUBLIC NOTICE. WILL INJECT GAS AND FLUID, NOT JUST FLUID
Annulus Pressure Monitoring Approved 2000-08-11 RBDMS Rec
Last Compliance Report 2000-08-14 RBDMS Rec
Completion Report Received 2000-08-24 RBDMS Rec
APP 2009-11-30 Proposed Formations:GREENFIELD DOLOMITE, Issued Date:11/30/2009, Expired Date:11/30/2010 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:SWD, Proposed Well Class:SWIW
Plugged/Abandoned 2010-11-15 RBDMS Rec
Construction Permit Expires 2010-11-30 RBDMS Rec
Record Last Modified 2015-09-24 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-11-20 1530 1538 16
1530 1538 16
1530 1538 16

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 28 1200 Gal 0

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1019836467 2009-3-3 0:00:0 SW No Violations
-1297869539 2005-2-22 0:00: SW No Violations
-1306801169 2007-3-29 0:00: SW No Violations
-1390336797 2008-3-19 0:00: SW No Violations
-1439157658 2007-5-22 0:00: SW No Violations
-1686574833 2006-12-4 0:00: SW No Violations
-1746561941 2002-10-28 0:00 SW No Violations
-1925536445 2006-5-30 0:00: SW No Violations
-2143064336 2007-8-6 0:00:0 SW No Violations
-80809303 2008-9-9 0:00:0 SW No Violations
-810659753 2010-11-16 0:00 PB No Violations
-816773588 2006-3-27 0:00: SW No Violations
-892700149 2006-1-26 0:00: SW No Violations
0000PL5725 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0080809303 2008-09-09 Salt Water Injection Well No Violations Inspect well and location with Jeff Fry. ID posted. No meter.
0309024007 2003-05-06 Salt Water Injection Well No Violations Meet with representative Chad Delbecq of Ohio EPA Air. Regarding the potential release of h2s.
0325103488 2003-08-27 Salt Water Injection Well No Violations Inspect Well. Dike area for tank are 3/4 full.
0390680496 2010-09-13 Salt Water Injection Well No Violations inspect well and location. Well in bean field. All production equipment removed from location.
0434096540 2008-01-28 Salt Water Injection Well No Violations Inspect well. Lease lane to well has been blocked by several dump truck loads of tree stump debris. Well shut in.
0616188674 2005-07-27 Salt Water Injection Well No Violations Inspect Well. No ID at Tank. Water in dike.
0775561514 2007-11-14 Salt Water Injection Well No Violations Inspect facility. Site ok.
0810659753 2010-11-16 Plug / Plug Back No Violations Inspect well. Well plugged, 28 joints of 4.5 inch casing on ground. Total of ~972 feet of pipe.
0816773588 2006-03-27 Salt Water Injection Well No Violations Inspect Well. Meter at tanks 07711 KwHr, meter #26550797. Dike area full water. 100 bbl tank is empty. 210 bbl tank appears to have fluid in it.
0892700149 2006-01-26 Salt Water Injection Well No Violations Inspect well and tanks. Operator should install a needle valve to reduce the loss of annulus fluid and pressure when checked. Dike capacity is zero due to standing water.
0897664066 2009-04-06 Salt Water Injection Well No Violations Inspect well.
0909492866 2007-01-22 Salt Water Injection Well No Violations Inspect well. Well shut in.
1019836467 2009-03-03 Salt Water Injection Well No Violations Inspect well and location. Electric meter at pump 771 kwh.
1038597984 2002-11-29 Salt Water Injection Well No Violations Inspect Well. Annulus is at Zero PSI.
1043242920 2003-01-22 Salt Water Injection Well No Violations Inspect Well and Tank battery. Well has minimal injection pressure. Annulus is under pressure. 210 bbl tank apparently was full with brine, and froze. Top and bottom of tank are compromised, expanded top and bottom out ward.
1046369743 2003-02-27 Salt Water Injection Well No Violations Well inspection. System idle.
1051106075 2003-04-23 Salt Water Injection Well No Violations Inspect Well and Tank battery Collect pressure reading for annulus. Transfer pump area has a brine separator. The Valve at base of vessel is closed and is dripping a solution. Collected sample and Quantab test for chloride. This solution appears not to be brine. Zero on the quantab, no change in color. A Gas vent line has been laid from a drip separator at the compressor pump to about 400 feet from the south (in the direction of the injection well). This line is open and laid on the ground to allow the H2S laden vapors to dissipate. The Ground is saturated with residual brine and the vegetation is burned. At the terminus of the line the ground is stained black due to the H2S. Reading on the meter un the vicinity of the line terminus were near 10-14 ppm.

Vapor reading in the immediate vicinity of the of the pump unit exceeded 35 ppm. And, Reading about 40 feet south of pump were greater than 10 ppm.

1065191722 2003-10-03 Salt Water Injection Well No Violations ID at well head. Well annulus at 0 pressure. Spoke with Dave Houghton at nearby well site that was being plugged today.(PN 720).
1066397054 2003-10-14 Salt Water Injection Well No Violations Inspection w/ J Fry. Slight difference noted in pressures between annular and casing. The operator should schedule a 200 # pressure test monthly in order to verifiy the integrity of the well. Inspector should be notified ahead of time so it can be witnessed . (614) 205-0032
1078401880 2009-06-03 Salt Water Injection Well No Violations Inspect well. Cattails are growing in dike area. Electrical meter 07711.87Kw hr.
1082990515 2004-04-26 Salt Water Injection Well No Violations Inspect Well. ID posted.
1088619766 2004-06-22 Salt Water Injection Well No Violations Inspect injection well. Nipple on injection line is rusted. Dike is full with water and oil.
1093350712 2004-08-23 Salt Water Injection Well Violations Noted Inspect Well and Tanks. Nipple on production line at well head is rusting and should be replaced. Needle valve for Gauge needs to be replaced. Lane to well needs mowed. A path should be cleared above the product line from the tanks to well. The dike has standing water and free oil accumulated in dike area, needs to be cleaned up. Fluids have breached dike and burned an area about 200 sq. yds.
1099494474 2004-11-03 Salt Water Injection Well No Violations Inspect Well. ID Posted. Site looks ok.
1104841289 2004-12-27 Salt Water Injection Well No Violations Inspect injection well and tanks. Tanks frozen. Walk line although covered with snow during inspection.
1115722466 2005-04-28 Salt Water Injection Well No Violations Inspect well. Dike is full with water.
1128512323 2005-09-28 Salt Water Injection Well No Violations ID posted. Dike area half full with water.
1140095901 2006-02-14 Salt Water Injection Well No Violations The Division Requested the operator to pressure up and test annular space. Witnessed 15 minute mini test at 500 psi.
1154183647 2006-07-24 Salt Water Injection Well No Violations Inspect Well. No change to well head setup.
1159360127 2006-09-27 Salt Water Injection Well No Violations There was no needle valve on annulus. There were fluids in the pit.
1170421285 2007-01-12 Salt Water Injection Well No Violations Inspect tank battery. Burn area south of tank about 40 feet by 75 feet. Area historicaly is wet.
1190635025 2007-09-24 Salt Water Injection Well No Violations Inspect well. Site ok. Operator should install a needle valve on annulus.
1210i27545 2001-11-28 Salt Water Injection Well No Violations Injection tank dike has rain water and will need pumped out. Checked over scrubber operations at plant. No H2S readings on meter. Heater stack operating. Gas compressor not running at this time.
1210i2754543 2001-11-28 0:00 SW No Violations
1210i35683 2002-03-20 Salt Water Injection Well No Violations Tanks and well appear ok. Walked to well.
1210i356833 2002-3-20 0:00: SW No Violations
1210i44554 2002-01-25 Salt Water Injection Well No Violations Surface facility and well ok. Walked line to well.
1210i4455445 2002-1-25 0:00: SW No Violations
1210i95187 2001-05-25 Salt Water Injection Well No Violations Storage tank dike has extra fluids due to heavy rainfall. Wellhead needs ID reposted. Talked about these to Bob Atha he will fix. Also annulus will be pressured up before scrubber station put on line per Bob.
1210i951874 2001-5-25 0:00: SW No Violations
1212493181 2008-06-03 Salt Water Injection Well No Violations inspect well and location. Site is idle.
1229002974 2008-12-10 Salt Water Injection Well No Violations Inspect well. Id posted.
1237287771 2005-11-21 Salt Water Injection Well No Violations Inspect well and location. Dike is half full with water. Injection system is incapable of production.
1248257973 2009-07-20 Salt Water Injection Well No Violations Inspect well. Site ok.
1253634168 2009-09-16 Salt Water Injection Well No Violations Inspect well and location. Well shut in.
1258649433 2009-11-19 Salt Water Injection Well No Violations Inspected well and measure pressure. The Landowner decided to dismantle and deconstruct the storage tanks and level the dike area. During his construction activity on 11/18/09 the local Fire department was contacted and arrived on site. The OEPA was contacted. Michael Dalton of OEPA was on site to inspect the site. Discussions with Joe OHail determined that grading out the area and adding some lime would be sufficient for any contamination and that there was little risk of impact to the environment. Mr. OHail said he would contact Mr. Dalton when he had the site graded. MRM contacted Bob Atha and apprised of situation, advised that the installation of a brine disposal facility should be installed or the reaming well should be plugged and abandoned.
1288881559 2010-11-04 Salt Water Injection Well No Violations On site to plug. (10:30 AM)

The site is vacant, no one around, no service rig.

1297869539 2005-02-22 Salt Water Injection Well No Violations Inspect Well. Pit full water. Advised operator to pump dry.
1306801169 2007-03-29 Salt Water Injection Well No Violations inspect well.
1329835757 2003-06-25 Salt Water Injection Well No Violations Inspect Well. Injection has positive pressure. Two inch valve on annulus for pressure gauge has a slight leak. Injection pipe run has rusting 90s at nipple.
1390336797 2008-03-19 Salt Water Injection Well No Violations Inspect facility. Walk line from well to tanks.
1439157658 2007-05-22 Salt Water Injection Well No Violations Inspect well. One 210 BBL tank and one 100 bbl tank.
1523624324 2008-07-28 Salt Water Injection Well No Violations Inspect location.
1543774917 2011-12-30 Final Restoration No Violations Inspected location. Crop field. Restoration ok.
1686574833 2006-12-04 Salt Water Injection Well No Violations Inspect well, location and test pressure. Dike area flooded. A 300 gallon plastic tote near aiming plant is leaking oil/brine onto the ground please empty contents.
1746561941 2002-10-28 Salt Water Injection Well No Violations Inspect well. Identification present and remarked as requested during the previous inspection. Condition of both valves are marginal. Annulus pressure of zero, need to test annulus monthly at a minimum pressure of 200 psi or maintain constant positive pressure that is different from the injection pressure.
1925536445 2006-05-30 Salt Water Injection Well No Violations Inspect Well. Operator is recommended to install a needle valve on the annulus to reduce the loss of fluids/ inhibitor and pressure.
2006768494 2004-10-04 Salt Water Injection Well No Violations Inspect tank battery. Free standing oil has been cleaned up. Closed NOV of 8/23/04. Bung at base of 210 bbl tank may be breached. A rag was stuffed into bung hole. Tank has experienced an internal explosion and the top and bottom of tank are deformed. Operator is advised to scrap tank prior to continued use.
2143064336 2007-08-06 Salt Water Injection Well No Violations Inspect well. Site ok.
2787486041 2004-01-20 Salt Water Injection Well No Violations Scrubber station idle. Could not check pressures today. Tanks were overtopping with oil but fluid was contained in dike. Dave Atha was notified by voicemail of the problem.
278748604105865 2004-1-20 0:00: SW No Violations
278748604113523 2004-1-20 0:00: PW No Violations
309024007 2003-5-6 0:00:0 SW No Violations
325103488 2003-8-27 0:00: SW No Violations
390680496 2010-9-13 0:00: SW No Violations
434096540 2008-1-28 0:00: SW No Violations
616188674 2005-7-27 0:00: SW No Violations
775561514 2007-11-14 0:00 SW No Violations
897664066 2009-4-6 0:00:0 SW No Violations
909492866 2007-1-22 0:00: SW No Violations
PL5725 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1093350712 US-OH-102209 2004-08-24 Pollution/Contamination

For data sources see[5]

References