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34-083-22486

Well Details

Well ID: 34-083-22486
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Country: United States
State: Ohio
County: Knox
Municipality: Morris Township
Operator Name: GRAHAM PUMP SERVICE
Well Pad ID:
Farm/Lease Name: MCCELLAN ROBERT & DELORES
License Status: Final Restoration
License Date: 2006-05-03
Spud Date: 1978-02-03
Spud Drilling Contractor:
Final Drill Date: 1978-02-25
Well Total Depth: 2130.00 ft
Configuration: Vertical
Latitude: 40.430000
Longitude: -82.530000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1978-02-03 CHANGED STATUS FROM BLANK TO PR , CORRECTED Y COOR., AND CHG TD DATE FROM 12/29/2003. 5/3/06. JG
Reached Total Depth 1978-02-25 CHANGED STATUS FROM BLANK TO PR , CORRECTED Y COOR., AND CHG TD DATE FROM 12/29/2003. 5/3/06. JG
CO 1982-10-28 123 GUARDIAN MANAGEMENT INC GeoDate 10/28/82
Unknown 1982-10-28 Issued Date 10/28/82 Expired Date 4/26/83 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Change of Owner 1999-04-27 Operator changed from 123, GUARDIAN MANAGEMENT INC to 6434, GRAHAM PUMP SERVICE
Completed 2003-12-29 CHANGED STATUS FROM BLANK TO PR , CORRECTED Y COOR., AND CHG TD DATE FROM 12/29/2003. 5/3/06. JG
APP 2003-12-30 Proposed Formations:CLINTON, Issued Date:12/30/2003, Expired Date:12/29/2004 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
APP 2006-05-03 Proposed Formations:CLINTON, Issued Date:5/3/2006, Expired Date:5/3/2007 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2007-05-03 CHANGED STATUS FROM BLANK TO PR , CORRECTED Y COOR., AND CHG TD DATE FROM 12/29/2003. 5/3/06. JG
Plugged/Abandoned 2007-05-21 CHANGED STATUS FROM BLANK TO PR , CORRECTED Y COOR., AND CHG TD DATE FROM 12/29/2003. 5/3/06. JG
Record Last Modified 2013-03-14 CHANGED STATUS FROM BLANK TO PR , CORRECTED Y COOR., AND CHG TD DATE FROM 12/29/2003. 5/3/06. JG

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 600 Bbl 0

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-119727879 2007-5-7 0:00:0 PB No Violations
-1346310510 2003-4-24 0:00: PW No Violations
-1911369861 2006-4-24 0:00: AM No Violations
0119727879 2007-05-07 Plug / Plug Back No Violations Pipe on site to run over top of 1 1/2 inch pipe that tore in two at 1300 ft.
0597901053 2003-12-08 Production Wells No Violations Leak repaired, well still incapable
1070462326 2003-12-03 Production Wells Violations Noted Received call from landowner Dan Galbrieth re: salt water leaking from well head. Inspection revealed steady stream of brine water coming from well head with signs of vegetation kill in a 3 foot circle around well. Stream is nearby but not impacted. Well owned by Paul Graham Pump Service. Phone message was left to Paul Graham. The soil around well head needs to be cleaned up and well either needs to be plugged or made capable to produce.
1073054669 2004-01-02 Production Wells No Violations Well has leaked brine in past. Operator has applied for a permit to plug. Dave Crow left a voice mail message on my cell phone would be plugging this morning 8:00 am. I have no plug permit for this well.

No activity at well site, well not leaking. Calle

1077295028 2004-02-20 Production Wells No Violations Well head not leaking after temporary repair. Plugging permit has been issued and is good for one year.
1103291795 2004-12-17 Production Wells No Violations Well is not capable. Outside 4 casing that is sticking up in air has deteriorated more and is in poor condition. This well had leaked previously. Plug permit expires 12-29-04. Took 1 digital photo. Have tried contacting Paul Graham, he wont return my phone calls.
1107282247 2005-02-01 Production Wells No Violations Plugging permit expired in Dec 2004. Paul Graham was contacted by Jeff Fry, Supervisor. Operator has had trouble getting someone that is available to plug well. No change noted on site today.
1178554328 2007-05-04 Plug / Plug Back No Violations 1 1/2 inch tubing came apart at 1300 ft. Salt water is present behind 4 1/2 inch. Will need to run pipe over 1 1/2 and cement bottom.
1178554328212302 2007-5-4 0:00:0 PB No Violations
1224790781 2008-10-23 Final Restoration No Violations Well has been plugged. NOV terminated. Final restoration passes. Area is cropfield.
1346310510 2003-04-24 Production Wells No Violations With Paul Graham to help him locate the well. No pumpint unit or storage facilities. He is going to apply for a plugging permit and plug the well.
1911369861 2006-04-24 Administrative Inspection No Violations Well is still not producing or plugged per NOV. Requested Chiefs Order today.
597901053 2003-12-8 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1070462326 US-OH-101464 2003-12-03 Well operation causing pollution and contamination
1070462326 US-OH-101465 2003-12-03 Well shall be plugged

For data sources see[4]

References