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34-167-27274

Well Details

Well ID: 34-167-27274
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Country: United States
State: Ohio
County: Washington
Municipality: Palmer Township
Operator Name: AM-TEK OIL INC
Well Pad ID:
Farm/Lease Name: TEPE RALPH
License Status: Producing
License Date: 1982-08-25
Spud Date: 1982-09-04
Spud Drilling Contractor: KINGFISHER EXPL
Final Drill Date: 1982-09-28
Well Total Depth: 1829.00 ft
Configuration: Vertical
Latitude: 39.430000
Longitude: -81.700000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1982-08-25 605 DOVER OIL CO GeoDate 8/25/82
Oil and Gas 1982-08-25 Issued Date 8/25/82 Expired Date 2/15/83 Acres 0201500 Tool Type CT Proposed Formation OHIO SHALE Proposed Depth 01829 Proposed Drill Depth 01829
Original Spud 1982-09-04 FILED FOR SECTION 107 TIGHT FM CREDIT: APPROVED & SENT TO FERC 7-12-01
Completed 1982-09-28 FILED FOR SECTION 107 TIGHT FM CREDIT: APPROVED & SENT TO FERC 7-12-01
Reached Total Depth 1982-09-28 FILED FOR SECTION 107 TIGHT FM CREDIT: APPROVED & SENT TO FERC 7-12-01
Completion Report Received 1983-01-10 FILED FOR SECTION 107 TIGHT FM CREDIT: APPROVED & SENT TO FERC 7-12-01
Construction Permit Expires 1983-02-15 FILED FOR SECTION 107 TIGHT FM CREDIT: APPROVED & SENT TO FERC 7-12-01
Change of Owner 2000-01-10 Operator changed from 605, DOVER OIL CO to 3434, GONZOIL INC
Change of Owner 2008-08-14 Operator changed from 3434, GONZOIL INC to 8404, CONLEY ENERGY CO LLC
Record Last Modified 2017-02-15 FILED FOR SECTION 107 TIGHT FM CREDIT: APPROVED & SENT TO FERC 7-12-01

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2001-07-12 1768 1771 10
1768 1771 10
1768 1771 10

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 110 Mscf 0
H2O 0 1500 Bbl 50000 110 MSCF N2 ASSIST

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 DOVER OIL CO 331.00 680.00 0
1985 DOVER OIL CO 1660.00 488.00 0
1986 DOVER OIL CO 3518.00 299.00 365
1987 DOVER OIL CO 1519.00 118.00 365
1988 DOVER OIL CO 859.00 138.00 365
1989 DOVER OIL CO 2110.00 151.00 365
1990 DOVER OIL CO 2677.00 178.00 365
1991 DOVER OIL CO 2029.00 114.00 365
1992 DOVER OIL CO 1577.00 105.00 365
1993 DOVER OIL CO 1162.00 60.00 365
1994 DOVER OIL CO 871.00 76.00 365
1995 DOVER OIL CO 750.00 113.00 365
1996 DOVER OIL CO 433.00 77.00 365
1997 DOVER OIL CO 271.00 45.00 365
1998 DOVER OIL CO 245.00 83.00 365
1999 DOVER OIL CO 201.00 42.00 0
2000 GONZOIL INC 536.00 53.00 365
2001 GONZOIL INC 700.00 44.00 365
2002 GONZOIL INC 879.00 44.00 365
2003 GONZOIL INC 804.00 64.00 365
2004 GONZOIL INC 499.00 56.00 365
2005 GONZOIL INC 662.00 33.00 365
2006 GONZOIL INC 610.00 0.00 365
2007 GONZOIL INC 571.00 0.00 365
2008 GONZOIL INC 536.00 0.00 365
2009 CONLEY ENERGY CO LLC 786.00 70.00 323
2010 CONLEY ENERGY CO LLC 712.00 246.00 323
2011 CONLEY ENERGY CO LLC 381.00 97.00 324
2012 CONLEY ENERGY CO LLC 476.00 25.00 363
2013 CONLEY ENERGY CO LLC 463.00 37.00 365
2014 CONLEY ENERGY CO LLC 551.00 0.00 365
2015 CONLEY ENERGY CO LLC 376.00 28.00 365
2016 CONLEY ENERGY CO LLC 441.00 0.00 365
2017 CONLEY ENERGY CO LLC 86.00 27.00 365
2018 CONLEY ENERGY CO LLC 49.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 DOVER OIL CO Brine 0 0
1985 DOVER OIL CO Brine 0 0
1986 DOVER OIL CO Brine 0 365
1987 DOVER OIL CO Brine 0 365
1988 DOVER OIL CO Brine 0 365
1989 DOVER OIL CO Brine 0 365
1990 DOVER OIL CO Brine 0 365
1991 DOVER OIL CO Brine 0 365
1992 DOVER OIL CO Brine 0 365
1993 DOVER OIL CO Brine 0 365
1994 DOVER OIL CO Brine 0 365
1995 DOVER OIL CO Brine 0 365
1996 DOVER OIL CO Brine 0 365
1997 DOVER OIL CO Brine 0 365
1998 DOVER OIL CO Brine 0 365
1999 DOVER OIL CO Brine 0
2000 GONZOIL INC Brine 0 365
2001 GONZOIL INC Brine 165 365
2002 GONZOIL INC Brine 152 365
2003 GONZOIL INC Brine 82 365
2004 GONZOIL INC Brine 82 365
2005 GONZOIL INC Brine 298 365
2006 GONZOIL INC Brine 294 365
2007 GONZOIL INC Brine 275 365
2008 CONLEY ENERGY CO LLC Brine 0 181
2009 CONLEY ENERGY CO LLC Brine 0 323
2010 CONLEY ENERGY CO LLC Brine 0 323
2011 CONLEY ENERGY CO LLC Brine 0 324
2012 CONLEY ENERGY CO LLC Brine 34 363
2013 CONLEY ENERGY CO LLC Brine 0 365
2014 CONLEY ENERGY CO LLC Brine 80 365
2015 CONLEY ENERGY CO LLC Brine 160 365
2016 CONLEY ENERGY CO LLC Brine 0 365
2017 CONLEY ENERGY CO LLC Brine 0 365
2018 CONLEY ENERGY CO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1162035856 2009-7-31 0:00: PW No Violations
-1724541357 2009-7-9 0:00:0 PW No Violations
0000PL1935 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0914764353 2015-04-21 Production Wells No Violations Upon inspection, it was observed that this well is capable of production and is producing. The well consists of a pumping unit standing over 4.5 casing and 2.375 tubing. The well is producing on the tubing. The tank battery consists of a 210 bbl production tank, mechanical separator, drip, meter run, and containment dike. Legible and correct ID information is posted on the tank. The containment dike has been breached in the past and an old brine kill area approximately 50x50 is present downhill from the tank battery. Previous inspection reports indicate that this has been a persistent issue. I will contact Conley Energy and instruct them to till in lime and fertilizer with the soil 2-3 times and seed and mulch the area again to encourage growth.
0953956760 2009-07-31 Production Wells No Violations Inspection this day found well with jack, location has been cleaned up. Now has nice dike around the tank, tank replaced? Ground below the tank has been smoothed, limed, reseeded and mulched and grass starting to grow. Pleased with the job that they did.
1125452857 2007-04-13 Production Wells No Violations Inspection this day found well producing with jack, tank has good IDs, no dike, small pit behind that has water. Hillside below tank very eroded - red clay so probably wont grow much but appears may have dumped some water over time. Told them to get dozer over, smooth up hillside and replant with grass or something that will keep it from eroding.
1162035856 2009-07-31 Production Wells No Violations Inspection this day found tank had been replaced, dike built back up and kill area below the tank has been limed, seeded and mulched. Current chart in meter, still needs to get IDs up.
1724541357 2009-07-09 Production Wells No Violations Inspection this day found well producing with jack, current chart in meter, stock tank dripping brine from bottom valves into small pit. Large kill area below the tanks where water have been run in the past. Called Bob Dunbarger and asked him to clean up kill area, scatter lime, till in and plant grass seed. Needs more dike around tanks.
914764353 2015-4-21 0:00: PW No Violations 1.00
953956760 2009-7-31 0:00: PW No Violations
PL1935 PL No Violations

For data sources see[9]

References