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Well ID: 34-169-23798 |
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Farm/Lease Name: |
First Permit Date: |
Last Permit Date: |
Spud Date: |
Unconventional: |
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Producing: |
Violations: |
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Longitude: |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1757951532 | 2013-04-02 | Appears to be in compliance. | ||||
-1808441755 | 2011-06-21 | Plug well with Thompson Well ser. and Petroset cementing. Could only get bottom plug set today could not get casing to rip. | ||||
-357418734 | 2011-07-05 | Pipe has been cut off with no leaks found. Pits are empty ready to close. Area needs graded and seeded. | ||||
1617974722 | 2011-06-22 | Met with Inspectors Grimm, Wallace, Murphy. Plug well to surface with Thompson Well and Petroset cementing. Rip 4 1/2 casing at 2700 ft and use casing to set remaining plugs. | ||||
PL701 | Preliminary Restoration done information from Data Point |