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34-105-23602

Well Details

Well ID: 34-105-23602
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional:
Horizontal:
Producing:
Violations:
Latitude:
Longitude:

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1484725055 2013-02-19 Well equipped with a pumping unit with a gas engine. The valves on the production casing and the tubing were open. Well has good identification.
1189005327 2007-09-04 Witnessed the cementing of the surface casing. A good return was observed and the cement appeared to stay at the top.
1345522693 2007-09-18 Drilling on fluid at approximately 1600 feet. All conditions were acceptable.
1569080891 2012-10-10 Annular Disposal Mechanical Integrity Test. Jeff Burke tested the annulus three times using nitrogen. All three tests failed to maintain pressure of 204 psi. Jeff Burke disconnected the annular disposal line at the wellhead and is storing the brine in a 100 barrel steel tank.