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Well ID: 34-105-23602 |
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Last Permit Date: |
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Unconventional: |
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Producing: |
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PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1484725055 | 2013-02-19 | Well equipped with a pumping unit with a gas engine. The valves on the production casing and the tubing were open. Well has good identification. | ||||
1189005327 | 2007-09-04 | Witnessed the cementing of the surface casing. A good return was observed and the cement appeared to stay at the top. | ||||
1345522693 | 2007-09-18 | Drilling on fluid at approximately 1600 feet. All conditions were acceptable. | ||||
1569080891 | 2012-10-10 | Annular Disposal Mechanical Integrity Test. Jeff Burke tested the annulus three times using nitrogen. All three tests failed to maintain pressure of 204 psi. Jeff Burke disconnected the annular disposal line at the wellhead and is storing the brine in a 100 barrel steel tank. |