INSPECTION ID
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DATE
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DESCRIPTION
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COMMENT
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VIOLATION ID
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VIOLATION CODE
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VIOLATION_COMMENT
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-140445405
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2008-10-06
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Inspect well location. Test casing head with gas meter. The gas is 100% LEL at rim of riser pipe. The records indicate the original rock pressure was 200 psi after shut in for 48 hours.
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-1679807970
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2009-12-29
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Inspect well. Measure H2S at greater than 16 ppm and LEL greater than 41 ppm. Well head cut off. Open 16 inch riser pipe marks location. Gas is free flowing from well. Previously reported by landowner that neighbor indicated smell of H2S on calm nights.
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-1961045828
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2009-03-23
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The marker pipe is full with water, gas is boiling out. Measure reading with meter LEL 34% and H2S >10ppm
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1223322017
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2008-09-29
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Contacted by Rick Judge of Siteworks Drilling on behalf of Neal Johannsen the landowner. The landowner and neighbor reported odors over time and a burn area in field where crops will not grow. Landowner excavated burn area under supervision of DMRM and located the following items during the excavation process. Ground that was stained, segments of 2 inch pipe, segments of 1 inch pipe with regulator, severed orange gas line in direction of former landowner residence of 2717 Court Rd. A 9 foot segment of 8 inch casing cut off with a cutting torch, a 10.5 foot segment of 8 inch casing with swage and 2 inch cap that was intact, and remnants of numerous Baroid hole plug bags. During excavation Bentonite was observed in the former excavation. The original well was located 10 feet below grade. The borehole was filled with bentonite to within 2.5 feet of the top of 8 inch steel casing. A 12 inch drain pipe was fitted over the well and backfilled for later location. Some gas was leaking from well. During site activities it was reported by the current landowner that there would be no negotiations for purchase with a well on the property. Also, reported the previous landowner may have contacted Tibboles Well Drilling, Inc. a water well driller in Bellevue, Ohio for plugging of the well.
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1223473406
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2008-09-30
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Inspect well location. Hartland Twp, SE1/4 SE1/4 Section 3, Lot 11 Use gas meter to collect readings; On ground near pipe head, 4% LEL and 1 ppm H2S. At top of pipe, 49% LEL and 19 ppm H2S. In pipe, 82 % LEL and 29 ppm H2S. Wind about 5 to 7 mph from west, temp upper 50's. Rain over night filled lower portion of excavation. Well is degassing uncontrolled.
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1224190118
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2008-10-14
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Inspect well location. Well continues to release gas uncontrolled from riser pipe. Readings at well head zero. Reading at lip of riser pipe exceed LEL at 100% and H2S at 22 ppm. Windy out of west about 7 to 10 mph.
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1230026919
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2008-10-01
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Inspect well location. Gas continues to release from borehole uncontrolled and boil water in former excavation.
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1375807059
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2013-08-05
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An inspection of this orphan well revealed the release of H2S from inside a 14.5" outside diameter black corrugated pipe. The fluid within the pipe was near the surface and contained a strong and constant flow of gas to the surface. Note: A layer of gray film was also observed on the surface of fluid. The well was monitored with a gas detector equipped with an automatic pump, a probe and filter. The following concentrations were noted during the inspection: H2S= 30; CH4= 3.54; and the LEL was exceeded. The well was situated on property designated as agricultural field with no crops planted at this time. The location contained two residential dwellings within approximately 500'. The well location did not contain any overhead obstructions or oilfield debris. A GPS reading was obtained and recorded for the well and potential entry off Court Rd. Central Office will be notified of H2S status for this township.
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