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Well ID: 34-155-23910 |
County: |
Municipality: |
Operator Name: |
Well Pad ID: |
Farm/Lease Name: |
First Permit Date: |
Last Permit Date: |
Spud Date: |
Unconventional: |
Horizontal: |
Producing: |
Violations: |
Latitude: |
Longitude: |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1015695652 | 2009-12-10 | no violations . | ||||
-1239155879 | 2014-04-24 | My inspection found the well in production. The well was equipped with a plunger lift unit. The tank battery consisted of a 210 barrel production tank and a separator. The dike met containment requirements. An identification sign was posted. A bull plug was installed on the load line. The lease road was in stable condition. | ||||
-275533530 | 2008-06-24 | Direct Drilling co. drilling at 2993' . | ||||
1134835132 | 2008-06-18 | Direct drilling , shut-down for repairs . Depth 857' . | ||||
1352408667 | 2008-06-16 | Direct Drlg. , depth 857' . Rig shut-down for repairs . | ||||
536676825 | 2008-06-20 | Direct Drilling still shut-down . Depth 857' . |