If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-035-22161 |
County: |
Municipality: |
Operator Name: |
Well Pad ID: |
Farm/Lease Name: |
First Permit Date: |
Last Permit Date: |
Spud Date: |
Unconventional: |
Horizontal: |
Producing: |
Violations: |
Latitude: |
Longitude: |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
-1069082899 | 2010-07-27 | Drilling at 2950' no violations. | ||||
-1192111588 | 2010-07-26 | drilling at 2750' no violation. | ||||
-1590005469 | 2010-07-22 | The drilling contractor was rigging up on the location. MRI 2 Norburt Lowder was on location, also. Conditions were acceptable. | ||||
-2008522404 | 2010-07-24 | BOP test passed | ||||
-224743257 | 2010-07-23 | Conductor cement operation was witnessed. The cement operation and site conditions were acceptable. | ||||
-418415170 | 2010-07-26 | Drilling on fluid at 1976' no gas encountered in oriskany top at 1946' | ||||
-504755703 | 2010-07-22 | Rig moving onto site. | ||||
-962128036 | 2010-07-23 | Surface casing was cemented. Cement operation and site conditions were satisfactory. | ||||
-99213477 | 2010-07-20 | Location made, orange fencing up around site perimeter, and silt fencing up per permit conditions. | ||||
1170344768 | 2010-07-29 | TD reached and running 4.5" casing rigging up to cement casing. | ||||
1282586478 | 2010-07-28 | Mrs. Veronica Gallo 440-446-0114 called to complain that they are drilling to close to homes at 31371 Cedar Road also she want to make sure the water table is protected . I arrived at site used GPS Checked spacing to home which is due south of well approximately 120'.
Checked casing program for what casing was set 72' of 11.75" conductor cemented on 7-23-10 no problem cementing,85/8" casing cemented on 7-23-10 no problems with cementing. Phone to Mrs. Gallou informed her that the well meets spacing and no problems encounter while cementing of the conductor and surface casing. Case#10-007 Case closed: |
||||
1322771487 | 2011-12-01 | Received complaint from resident 7 doors away of petroleum odor in water when opening spigot on outside of house. Scanned area with gas meter and obtained following readings. O2- 20.6/ LEL - 0/ H2S-0/CH4IR/ CO - 0. Company checked well pressure prior to 12:00 Noon and recorder 1 Lb pressure. | ||||
1323186307 | 2011-12-02 | Received notification from Norburt Lowder on 12/01/2011 of complaint of petroleum smell coming from outside water spigot when it is turned on. Residence is located at 31107 Cedar Road, Mayfield Heights, Ohio. Residence is located West of the oil and gas well, #34-135-2-2161-00-00. Well and tank battery were inspected, slight gas odor in air detected by smell when entering inside well head area. Used gas meter at waist level and around connections and fittings. The readings from the meter were as follows: O2-0/LEL-0/H2S-0/CH4IR/CO-0. Well head area and tank battery were inspected by the inspectors on site. Well is in compliance with 1501:9-9-05 | ||||
1351660189 | 2010-11-23 | |||||
633639835 | 2010-08-20 | Crew working on site fencing around tank battery and grading site out. |