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34-121-24477

Well Details

Well ID: 34-121-24477
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional:
Horizontal:
Producing:
Violations:
Latitude:
Longitude:

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-2043102973 2014-05-29 My inspection finds the drilling rig is at a current depth of 2086'. They anticipate a total depth of 2200'. The rig will then run 13.625" casing. A test of water in the northeast sump did not indicate any elevated chlorides.
-280300823 2014-05-30 My inspection today finds the drilling rig crew ran 13.375" casing to a depth of 2158'. Allied cemented the casing in place by circulating 1826 sks of class A cement into place. I witnessed 60 bbl of cement returns to surface. The casing integrity pressure test passed.
-326386571 2014-07-29 My inspection today finds Allied Oil and Gas Services just finished the 5.5" casing cement job. Patterson rig 343 ran 18070' of twenty pound 5.5" casing with centralizers placed on every other joint in the lateral section. Allied cemented the casing in place with 1970 sacks of class H cement. The cement report indicated that 70 barrels of a 262 barrel spacer were returned to surface indicating adequate cement coverage.
-422395062 2014-06-04 My inspection today finds the Patterson Drilling rig 343 has drilled 12.35" hole to a depth of 7252'. They will run 9.625" casing to bottom and Halliburton will cement the casing in place.
208110816 2014-03-29 My inspection today finds Express Energy drilled 100' of 32" hole. Express ran 100' of 26" casing and cemented it in place with 330 sks of class A cement. I verified the cement weight at 15.6 pounds per gallon. The cement stayed at surface and circulation was maintained through out the job.
97313257 2014-06-05 My inspection today finds the rig ran 7251' of 9.625" casing. Halliburton is cementing the casing in place with Extendacem and Halcem.