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Well ID: 34-031-21696 |
County: |
Municipality: |
Operator Name: |
Well Pad ID: |
Farm/Lease Name: |
First Permit Date: |
Last Permit Date: |
Spud Date: |
Unconventional: |
Horizontal: |
Producing: |
Violations: |
Latitude: |
Longitude: |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-115253986 | 2007-08-15 | Echo meter test for fluid level in well . | ||||
-1962584569 | 2013-01-03 | On site to witness fluid level testing with echo meter along with well owner and tester Jim Gessel. | ||||
-2077529634 | 2005-12-16 | Witnessed shooting of ecometer by Jim Gessel of Dome Drilling for static fluid test w/ J Fry. | ||||
-819375685 | 2011-05-09 | Echo meter test. | ||||
1282263826 | 2012-12-14 | On the day of my inspection I found that the well head was equipped with a pumping unit and connected to a tank battery that consisted of one 100 barrel stock tank, one 100 barrel brine tank, one knock-out tank and an earthen dike. Proper identification was posted and there were no leaks or spills at the well head or tank battery. This well shares a tank battery with permit 1692. No violations at this time. | ||||
221507821 | 2004-08-20 | TESTED 100# DEEP COLLAR CLINTON WELL | ||||
689075488 | 2003-12-16 | Well in production . |