INSPECTION ID
|
DATE
|
DESCRIPTION
|
COMMENT
|
VIOLATION ID
|
VIOLATION CODE
|
VIOLATION_COMMENT
|
-1607309813
|
2009-08-18
|
|
There is no pumping unit on the wellhead. The well is not capable of production. There is no form of identification posted at the well head. The well has rods and tubing in it.
|
|
9-9-05(A)10
|
|
-1607309813
|
2009-08-18
|
|
There is no pumping unit on the wellhead. The well is not capable of production. There is no form of identification posted at the well head. The well has rods and tubing in it.
|
|
NONE
|
|
-845038514
|
2009-08-18
|
|
FOLLOW UP TO NOV # -1607309813 There is no pumping unit on the wellhead. The well is not capable of production. There is no form of identification posted at the well head. The well has rods and tubing in it.
|
|
|
|
1394759192
|
2012-07-18
|
|
An inspection of plugging activity revealed Mr. Nathan Nethers was pulling the 7" casing from the wellbore. The first half of clay bottom plug was set yesterday and was not witnessed. All casing was retrieved today and witnessed clay washed to the surface. Instructed well owner, Mr. Gary Nethers to leave wellbore and allow clay to settle for a couple days.
|
|
|
|
1440241239
|
2013-07-11
|
|
This inspection was conducted as a final restoration status check. The inspection revealed oil field debris has been left at the well location. The lease road has not been restored. Final restoration does not meet ORC 1509.072. Well owner will be notified of inspection and will need to finish restoration.
|
|
|
|
PL13713
|
|
|
Preliminary Restoration done information from Data Point
|
|
|
|