X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-127-21530

Well Details

Well ID: 34-127-21530
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional:
Horizontal:
Producing:
Violations:
Latitude:
Longitude:

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1227159543 2011-06-02 Accompanied D. Goins on restoration follow-up.
-1941600534 2011-06-02 Restoration meets 1509.072(B) requirements.
-2132501503 2010-04-20 No circulation at start up, pumped approx. 200bbls of water. Able to get circulation back on well bore, started cleaning out well bore. Approx.275'ft hit rock bridge plug, after drilling out bridge plug encountered small amount of gas and water. Continued cleaning out well bore at approx. 400'ft lost circulation. Pumped approx.125 bbls of water down well bore and shut in for the night.
-643910373 2010-01-06 Pre-bid meeting at well site, met with Rob Stonerock, Mike McCormac, Ken Wright and Ben Lehner, no change in well since last inspection.
-937858483 2010-04-07 Plugging rig will be moving in next week.
-946318802 2010-04-21 At start up pumped over 300 bbls of water in well bore, no circulation. Built another pit and started mixing gel, and lost circulation materials for LCM pill. Pumped LCM pill down well bore and started cleaning out well bore, still no circulation. Mixed up another LCM pill and pumped down well bore, left set over night.
1074707834 2010-04-22 Started cleaning down well bore, after pumping approx. 20 bbls of fluid in well bore circulation was losted. Tripped out of well and reduced bit size to a 6 1/4", tripped back in continued cleaning down well bore with no circulation. Pumped approx 200 bbls of water with no circulation. Cleaned down to approx. 1135'ft., with no circulation.
1137272568 2009-08-24 Marked well location and lease road for pre-bid meeting.
1273750107 2010-04-16 Cleaning out well bore with a 8 3/4" button bit. Drilling out wood and plug materials. At the end of the day approx. 80'ft deep.
1273841312 2010-04-23 Spoke with Mike McCormac about plugging well at 1135'ft, company has fears that if they continue down well bore without circulation that materials may stick bit anad drill pipe. No shows of gas since first drilling through rock bidge plug. Pulled drill pipe and bit, ran in 1 1/2" tubing in well bore. Cemented well bore soild from 1135'ft to 170'ft. Will leave set over weekend will tap plug next week.
1273842282 2010-04-27 Tagged plug, plug set at 210'ft. Set Brush and stone bridge plug at 210'ft over coal seam. Topped off well with approx. 6 yards of 9 bag grout mix.
1435798528 2010-04-19 Started cleaning out well bore, at approx. 170'ft lost circulation, recovered after pumping approx. 100bbl of brine. At approx. 223'ft drilling hard material, at 225'ft lost circulation, unable to recover.
1722440352 2010-04-01 Started to remove trees and brush and prepare well site for plugging rig.
1966972584 2010-04-29 Witnessed cutting off conductor casing and placing ID plate on well bore.
870726645 2007-04-18 Met with Mike McCormac and Max Norris(WNF) to inspect orphan well, no casing visible in well, open well bore, approx 16" across. Fluid level approx 50'ft down. No contamination noted at this time. With an open hole like this in public area this well may cause harm to the public.
956882573 2008-02-26 Follow-up inspection, took photos and sketch for I&O case.