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34-035-22156

Well Details

Well ID: 34-035-22156
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional:
Horizontal:
Producing:
Violations:
Latitude:
Longitude:

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1086050813 2010-04-10 cemented conductor.
-1366610896 2010-04-17 3611 feet of production casing was installed and cemented.
-1450037862 2012-03-06 No violations found, well is in compliance.
-1844262776 2010-04-11 surface cementing good returns to surface.
-458768987 2010-04-11 On site for BOP test. Closed BOP at 350psi, pressured hole to 190psi, test was for 15 minutes, 10psi pressure lose during test, 5.2% lose of pressure BOP passed. Pits and linear were in good repair. Safety fence was up. Permit was posted in the dog house. Two fire extinguishers in the dog house (charged), one on the boom (not inspected), one on the mud pump (charged) and one by the engine on the rig (charged). Site was in good repair.
-875953674 2010-04-12 Drilling at 1120' No odors present checked with gas meter no readings

No violation.

1682073566 2010-03-29 Held on site meeting to discuss the on site construction and permitn conditions.
1786623495 2010-04-11 cemented conductor casing.
1955290958 2010-03-29 Held presite meeting to discuss permit conditions for the well.
1958162413 2010-04-27 meeting at Uniontown office to review bond log because cement not covering lockport by 100' meeting determined not gas encountered in newburg zone. Rick Simmer Oked company to proceed with stimulation of well.
2083899026 2013-07-24 The producing unit consists of a wellhead with mechanical plunger-lift unit and above-ground storage tank (AST) battery, The wellhead is located in a board-on-board enclosure which is locked. The well is currently producing. There is not ID at the wellhead. I did not observe any signs of leakage or problems. The AST battery is comprised of one 140-barrel production tank, one 50-barrel brine tank, and mechanical separator in a board-on-board enclosure. There is a unit ID at the wellhead. Secondary containment is good.
2132032583 2010-06-01 Ground leveled around well siteand an temporary fencing (chain link) up around well.
818618918 2011-12-28 On 12/28/2012, DNR Inspector Richard Skidmore completed an urban preliminary restoration well inspection for DNR Inspector Ray Wallace. The lease road, tank battery, and well head locations are in compliance with 1501:9-9-05. Inspection passed.