INSPECTION ID
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DATE
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DESCRIPTION
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COMMENT
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VIOLATION ID
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VIOLATION CODE
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VIOLATION_COMMENT
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1331052107
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2012-03-01
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arrived on location and found well idle , no id posted and buried saltwater tank full. Within 30 days post id , empty saltwater tank, and place well into production or apply for plug permit.
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9-1-07
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1331052107
|
2012-03-01
|
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arrived on location and found well idle , no id posted and buried saltwater tank full. Within 30 days post id , empty saltwater tank, and place well into production or apply for plug permit.
|
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9-9-05(A)10
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1331052107
|
2012-03-01
|
|
arrived on location and found well idle , no id posted and buried saltwater tank full. Within 30 days post id , empty saltwater tank, and place well into production or apply for plug permit.
|
|
NONE18
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919270074
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2014-05-02
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|
On the day of my inspection following up on NOV-1331052107 and complaint id #3631, I witnessed that the well was equipped with 4.5 inch casing, 1.5 inch tubing, a plunger lift system and a domestic gas hookup. Production equipment included a 210bbl tank, a concrete brine vault, a vertical separator and a 2 inch meter run with a .5 inch orifice and a chart recorder. Identification was not present and production records are current. Made phone call to Jeremy Caldwell of PAC Drilling, operator of well and I stated that identification needs to be updated to clear the current violation on the well. Jeremy stated it would be up by the end of next week.
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936631306
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2014-04-09
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On the day of my inspection following up on NOV-1331052107, I witnessed that the well was equipped with 4.5 inch casing, 1.5 inch tubing, a plunger lift system and a domestic gas hookup. Production equipment included a 210bbl tank, a concrete brine vault, a vertical separator and a 2 inch meter run with a .5 inch orifice and a chart recorder. Contamination has been cleaned up and with production records current and meet the minimum for 2013. No identification was present.
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