X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-157-22985

Well Details

Well ID: 34-157-22985
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional:
Horizontal:
Producing:
Violations:
Latitude:
Longitude:

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1331052107 2012-03-01 arrived on location and found well idle , no id posted and buried saltwater tank full. Within 30 days post id , empty saltwater tank, and place well into production or apply for plug permit. 9-1-07
1331052107 2012-03-01 arrived on location and found well idle , no id posted and buried saltwater tank full. Within 30 days post id , empty saltwater tank, and place well into production or apply for plug permit. 9-9-05(A)10
1331052107 2012-03-01 arrived on location and found well idle , no id posted and buried saltwater tank full. Within 30 days post id , empty saltwater tank, and place well into production or apply for plug permit. NONE18
919270074 2014-05-02 On the day of my inspection following up on NOV-1331052107 and complaint id #3631, I witnessed that the well was equipped with 4.5 inch casing, 1.5 inch tubing, a plunger lift system and a domestic gas hookup. Production equipment included a 210bbl tank, a concrete brine vault, a vertical separator and a 2 inch meter run with a .5 inch orifice and a chart recorder. Identification was not present and production records are current. Made phone call to Jeremy Caldwell of PAC Drilling, operator of well and I stated that identification needs to be updated to clear the current violation on the well. Jeremy stated it would be up by the end of next week.
936631306 2014-04-09 On the day of my inspection following up on NOV-1331052107, I witnessed that the well was equipped with 4.5 inch casing, 1.5 inch tubing, a plunger lift system and a domestic gas hookup. Production equipment included a 210bbl tank, a concrete brine vault, a vertical separator and a 2 inch meter run with a .5 inch orifice and a chart recorder. Contamination has been cleaned up and with production records current and meet the minimum for 2013. No identification was present.