INSPECTION ID
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DATE
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DESCRIPTION
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COMMENT
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VIOLATION ID
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VIOLATION CODE
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VIOLATION_COMMENT
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-1739132816
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2007-11-16
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I preformed a rig inspection. Pit liners in good shape. The location was in good shape. There were no violations at this time.
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-1921128983
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2007-11-19
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I preformed a rig inspection. Pit liners in good shape. I called Greg New of Dorfman Production CO. and told him that order more cement for the long string and dump down the backside of the 8 5/8" casing. The drilling depth was 5035'. There were no violations at this time.
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1195478667
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2007-11-16
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I witnessed the cementing of the 8 5/8" casing. I found no violations at this time.
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1195669295
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2007-11-21
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I preformed a preliminary status check. Pit liners in good shape. The fluid level is down 2 foot from the top of the pits. Drilling equipment is still on location. This well does not pass preliminary restoration.
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1207051939
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2008-03-31
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I performed a preliminary restoration status check. The drilling rig equipment is gone. The debris has been removed. The drilling pits are closed. The top soil is still in piles. This well has not passed preliminary restoration.
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555063174
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2012-02-28
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I conducted a status check on this site and found that the well is equipped with a pumping unit and connects to a tank battery that consists of three 210 barrel stock tanks, two 100 barrel brine storage tanks, four separators, and an earthen dike. The tank battery is shared with permits 1277, 1278, 1406, 2544, 2504, and 2545. Proper identification was posted and I found no leaks or spills at the well head or tank battery. No violations at this time.
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817558958
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2008-04-23
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I performed a preliminary restorations status check. I GPS'd both the wellhead and the tank battery. The drilling pits are closed. The debris has been removed. Straw has been spread over the location and vegetation is starting to grow. This well has PASSED PRELIMINARY RESTORATION.
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