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| Well ID: 34-059-23548 |
| County: |
| Municipality: |
| Operator Name: |
| Well Pad ID: |
| Farm/Lease Name: |
| First Permit Date: |
| Last Permit Date: |
| Spud Date: |
| Unconventional: |
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| Producing: |
| Violations: |
| Latitude: |
| Longitude: |
| PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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| PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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| INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
|---|---|---|---|---|---|---|
| -1643247170 | 2002-12-30 | status check | ||||
| -1703029522 | 2014-07-16 | On the day of my inspection I witnessed that the site passed final restoration according to ORC 1509.072B. | ||||
| -1968532416 | 2014-03-17 | On the day of my inspection following up on NOV-276993868, I witnessed that the well has been plugged resolving issues. | ||||
| -222764481 | 2013-10-25 | This well is plugged. | ||||
| 1072070710 | 2003-12-19 | SERVICE RIG ON HOLE.EVALUATE WELL TO SEE IF CAASING HAS HOLE. WILLPUMP BOTTOM THRU TUBING. CASING HAS HOLE SOMWHERE DOWN HOLE. | ||||
| 1376671418 | 2013-08-16 | On the day of my inspection, I witnessed Cemenco displace thirty sacks of class A cement with a weight of 15.6 and a yeild of 1.18 at a depth of 5151' up to 4715', the pit is constructed and lined with tem mill black plastic up through the flow ditch and aroung the well head. | ||||
| 1376921352 | 2013-08-19 | |||||
| 1376931635 | 2013-08-19 | On the day of my inspection, I witnessed Davis Well Service rip the 4.5" production casing at a depth of 3760' and pull (1) joint of the 4.5" casing, at that point Cemenco displaced a 200' plug over the Big Lime formation, the rig crew then pulled fifty eight joints of 4.5" casing which took it up to the bottom of the 8.625" casing that is through the Berea Formation, Cemenco displaced a 200' plug, the rig crew then pulled seventeen joints of the 4.5" casing and checked the fluid level to see if it is 200' down, I instructed the crew to pull the remaining 4.5" casing, Cemenco displaced a 200' plug to surface, the rig crew was instructed to cut the 8.625" casing three foot below the ground level, place a cap with the permit number and the date on top of the well and cover with soil. | ||||
| 148792007 | 2004-09-20 | STATUS CHECK, PUMPING UNIT. WELLHEAD LAT/LONG REVISIONS ENTERED | ||||
| 1853579329 | 2008-09-10 | PRODUCING WELL. | ||||
| 276993868 | 2011-12-29 | FOLLOW UP TO NOV # 483674170 Upon receiving complaint from landowner Harry Kenney inspected site and found well shut in and no production reported since 2002,well is equipped with 11"conductor and 8" surface casing and 4.5" production casing and 1.5" tubing and 1-210 bbl tank in need of proper dike construction if well is placed into production. According to land owner lease has been cancelled and documents have been filed with county recorders office.
Plug well within 60 days or file for temporary inactive status if placed into production properly construct dike around tank and report production as required by law. Failure to comply may result in bond forfeiture. |
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| 483674170 | 2011-12-29 | Upon receiving complaint from landowner Harry Kenney inspected site and found well shut in and no production reported since 2002,well is equipped with 11"conductor and 8" surface casing and 4.5" production casing and 1.5" tubing and 1-210 bbl tank in need of proper dike construction if well is placed into production. According to land owner lease has been cancelled and documents have been filed with county recorders office.
Plug well within 60 days or file for temporary inactive status if placed into production properly construct dike around tank and report production as required by law. Failure to comply may result in bond forfeiture. |
9-9-05(A)10 | |||
| 483674170 | 2011-12-29 | Upon receiving complaint from landowner Harry Kenney inspected site and found well shut in and no production reported since 2002,well is equipped with 11"conductor and 8" surface casing and 4.5" production casing and 1.5" tubing and 1-210 bbl tank in need of proper dike construction if well is placed into production. According to land owner lease has been cancelled and documents have been filed with county recorders office.
Plug well within 60 days or file for temporary inactive status if placed into production properly construct dike around tank and report production as required by law. Failure to comply may result in bond forfeiture. |
9-9-05(A)9 | |||
| 483674170 | 2011-12-29 | Upon receiving complaint from landowner Harry Kenney inspected site and found well shut in and no production reported since 2002,well is equipped with 11"conductor and 8" surface casing and 4.5" production casing and 1.5" tubing and 1-210 bbl tank in need of proper dike construction if well is placed into production. According to land owner lease has been cancelled and documents have been filed with county recorders office.
Plug well within 60 days or file for temporary inactive status if placed into production properly construct dike around tank and report production as required by law. Failure to comply may result in bond forfeiture. |
NONE_ | |||
| 483674170 | 2011-12-29 | Upon receiving complaint from landowner Harry Kenney inspected site and found well shut in and no production reported since 2002,well is equipped with 11"conductor and 8" surface casing and 4.5" production casing and 1.5" tubing and 1-210 bbl tank in need of proper dike construction if well is placed into production. According to land owner lease has been cancelled and documents have been filed with county recorders office.
Plug well within 60 days or file for temporary inactive status if placed into production properly construct dike around tank and report production as required by law. Failure to comply may result in bond forfeiture. |
NONEC |