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34-059-23548

Well Details

Well ID: 34-059-23548
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional:
Horizontal:
Producing:
Violations:
Latitude:
Longitude:

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1643247170 2002-12-30 status check
-1703029522 2014-07-16 On the day of my inspection I witnessed that the site passed final restoration according to ORC 1509.072B.
-1968532416 2014-03-17 On the day of my inspection following up on NOV-276993868, I witnessed that the well has been plugged resolving issues.
-222764481 2013-10-25 This well is plugged.
1072070710 2003-12-19 SERVICE RIG ON HOLE.EVALUATE WELL TO SEE IF CAASING HAS HOLE. WILLPUMP BOTTOM THRU TUBING. CASING HAS HOLE SOMWHERE DOWN HOLE.
1376671418 2013-08-16 On the day of my inspection, I witnessed Cemenco displace thirty sacks of class A cement with a weight of 15.6 and a yeild of 1.18 at a depth of 5151' up to 4715', the pit is constructed and lined with tem mill black plastic up through the flow ditch and aroung the well head.
1376921352 2013-08-19
1376931635 2013-08-19 On the day of my inspection, I witnessed Davis Well Service rip the 4.5" production casing at a depth of 3760' and pull (1) joint of the 4.5" casing, at that point Cemenco displaced a 200' plug over the Big Lime formation, the rig crew then pulled fifty eight joints of 4.5" casing which took it up to the bottom of the 8.625" casing that is through the Berea Formation, Cemenco displaced a 200' plug, the rig crew then pulled seventeen joints of the 4.5" casing and checked the fluid level to see if it is 200' down, I instructed the crew to pull the remaining 4.5" casing, Cemenco displaced a 200' plug to surface, the rig crew was instructed to cut the 8.625" casing three foot below the ground level, place a cap with the permit number and the date on top of the well and cover with soil.
148792007 2004-09-20 STATUS CHECK, PUMPING UNIT. WELLHEAD LAT/LONG REVISIONS ENTERED
1853579329 2008-09-10 PRODUCING WELL.
276993868 2011-12-29 FOLLOW UP TO NOV # 483674170 Upon receiving complaint from landowner Harry Kenney inspected site and found well shut in and no production reported since 2002,well is equipped with 11"conductor and 8" surface casing and 4.5" production casing and 1.5" tubing and 1-210 bbl tank in need of proper dike construction if well is placed into production. According to land owner lease has been cancelled and documents have been filed with county recorders office.

Plug well within 60 days or file for temporary inactive status if placed into production properly construct dike around tank and report production as required by law. Failure to comply may result in bond forfeiture.

483674170 2011-12-29 Upon receiving complaint from landowner Harry Kenney inspected site and found well shut in and no production reported since 2002,well is equipped with 11"conductor and 8" surface casing and 4.5" production casing and 1.5" tubing and 1-210 bbl tank in need of proper dike construction if well is placed into production. According to land owner lease has been cancelled and documents have been filed with county recorders office.

Plug well within 60 days or file for temporary inactive status if placed into production properly construct dike around tank and report production as required by law. Failure to comply may result in bond forfeiture.

9-9-05(A)10
483674170 2011-12-29 Upon receiving complaint from landowner Harry Kenney inspected site and found well shut in and no production reported since 2002,well is equipped with 11"conductor and 8" surface casing and 4.5" production casing and 1.5" tubing and 1-210 bbl tank in need of proper dike construction if well is placed into production. According to land owner lease has been cancelled and documents have been filed with county recorders office.

Plug well within 60 days or file for temporary inactive status if placed into production properly construct dike around tank and report production as required by law. Failure to comply may result in bond forfeiture.

9-9-05(A)9
483674170 2011-12-29 Upon receiving complaint from landowner Harry Kenney inspected site and found well shut in and no production reported since 2002,well is equipped with 11"conductor and 8" surface casing and 4.5" production casing and 1.5" tubing and 1-210 bbl tank in need of proper dike construction if well is placed into production. According to land owner lease has been cancelled and documents have been filed with county recorders office.

Plug well within 60 days or file for temporary inactive status if placed into production properly construct dike around tank and report production as required by law. Failure to comply may result in bond forfeiture.

NONE_
483674170 2011-12-29 Upon receiving complaint from landowner Harry Kenney inspected site and found well shut in and no production reported since 2002,well is equipped with 11"conductor and 8" surface casing and 4.5" production casing and 1.5" tubing and 1-210 bbl tank in need of proper dike construction if well is placed into production. According to land owner lease has been cancelled and documents have been filed with county recorders office.

Plug well within 60 days or file for temporary inactive status if placed into production properly construct dike around tank and report production as required by law. Failure to comply may result in bond forfeiture.

NONEC