X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-055-20290

Well Details

Well ID: 34-055-20290
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional:
Horizontal:
Producing:
Violations:
Latitude:
Longitude:

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1062617311 2009-10-30 Lease road gate and lease road remain as well as 2nd gate at the turn to where the well was. A tree has grown up in front of the gate, gate can no longer be closed. There is a fence that runs parallel to the lease road, gate appears to be part of that fence. Debris from the north side of the gate was laying in the grass. Contacted John Flemming requested that the gate debris be removed gate be repaired or removed. Once land owner waivers have be/.en submitted for the lease road and the gates, restoration will be approved.
1221765477 2008-09-18 New chart in separator date on chart was 09/17/2008, no production shown on the chart. Tank battery has been cleaned up and lease road has been mowed. Area around well head has been mowed. Dike around tank battery is in good repair. Sign on tank battery needs repaired. Called John Flemming from company for status of the well. No production has been reported since 2000.
1228320900 2008-12-03 Lease road is stable and in good repair. Chart was put into separator in September of 2008. No production shown on chart. Valves are closed at the wellhead. Well is leaking around the 2.5 inch pipe. Called John Flemming, they are planning on plugging well. Informed John that I need to see a permit to plug within two weeks, or enforcement action will be taken.
1702309493 2009-02-12 Bill Fitzmartin from Range Resources on site at the time of inspection. Bill was making repairs to the well. Well is going to be put back into production, once repair parts are put into place.
1714533041 2009-05-19 On site for plug job. Operator set bottom plug through tubing. Operator pulled tubing, ripped 4.5" at 2955'. Pulled 4.5" joints to set lime plug. Operator attempted to break circulation, operator could not obtain circulation. Operator ran out of fluid, I requested lose circulation material be brought on site next day. Circulation needs to be obtained before lime plug is set. When operator shut down hole went on vacuum.
2125989170 2011-03-21 Site has been restored. Road remains, there are ruins of an old home in the woods near the tank battery location. Road was pre-existing. Fence has been repaired.
946339320 2010-08-10 Area has been graded, seeded and vegetation is established. Fence has been repaired. Lease is becoming vegetated. Final Restoration is passed.