INSPECTION ID
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DATE
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DESCRIPTION
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COMMENT
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VIOLATION ID
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VIOLATION CODE
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VIOLATION_COMMENT
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-1668082817
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2013-11-13
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This inspection was conducted as a standard production well status check. The well was equipped with a pumping unit and motor. The polish rod showed signs of recent production. It was not pumping during inspection. The tank battery consists of (2) 100 barrel tanks, gas separator, and drip. Note: (1) 1200 gallon plastic tank appears to be still in use. The top of the tank is busted. The tank had approximately 1 foot of fluid in it. Identification was not posted at the wellhead or tank battery. Weather: 33 degrees Sunny
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9-9-05(A)10
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-203497921
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2014-07-28
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The well has been plugged and violation resolved.
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-658825924
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2014-07-23
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Wheeler well service on site, rods and tubing have been pulled. 4.5 casing is producing gas. 8 tons of clay have been placed. All the 4.5 casing was pulled, 2213'. Inspector Brandom Mitchell is finishing this plug job.
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-69241330
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2014-07-24
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I witnessed plugging operations on this well. Mike Wheeler has been contracted to plug this well with clay for Mackenco. Refer to plug report for details.
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-942123913
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2014-07-25
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I witnessed plugging operations on this well. Mike Wheeler has been contracted to plug this well with clay for Mackenco. Refer to plug report for details.
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1407159796
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2014-07-28
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An inspection of plugging operations revealed that the well has been plugged. Clay could be seen at the surface. A GPS reading was obtained at the well.
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238066144
|
2014-07-16
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With Brandon Mitchell. Review well and records on pending water well investigation. See Brandon's report this date for details.
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VER1170
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1998-02-20
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