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Well ID: 34-111-20340 | Loading map...
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Producing: No | |
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Latitude: 39.8360512646 | |
Longitude: -81.2076126375 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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1401973545 | 2014-06-04 | The said well plugging began on 05/29/2014 with 2 tubing present inside 6.625 casing and Davis Well service rig on the hole, slim hole tools were ran inside the tubing showing a total depth of 1,722'- Appalachian wireline services were brought in on the same day and the tubing was shot off above the packer at 1,660' with a open hole packer at 1,678' to 1,1682', the 2 -11.5 V was recovered from 1,660' and the well plugged with 19 tons of clay and the casing cut off 30 below surface, all well related equipment and flowlines have been removed from the area. I also believe the well to be also historically identified as 3411163104 and at one point was assigned the current new 3411120340 api number. |