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Well ID: 34-127-25412 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1981-12-01 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 8 | |
Latitude: 39.7442038714 | |
Longitude: -82.3800678591 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1107336784 | 2012-08-30 | Huffman Bowers on site running 200' cement plug at 1940', this is being chased with 15 barrels fresh water gel, the gel is chased with 8 barrels of fresh water to allow the clay to work properly. All 4.5 pulled, 1940.' Clay washed in on top of the precast plug set at 900'. | ||||
-1599198207 | 2013-08-27 | Final restoration meets 1509.072. | ||||
-1747664447 | 2004-02-08 | FOLLOW UP TO NOV # 1076097397 No production for three years ( all equipment present ) pulleys are rusty. New GPS | NONE | |||
102678403 | 2012-07-23 | FOLLOW UP TO NOV # 826122208 The inspection revealed well is incapable of producing, according to Bruce Kellie(Owner) the down hole pump is stuck and will need a larger service rig to pull pump. According to landowner company had a service rig on well and was unable to remove stuck pump and removed rig without placing well into production. No production has been reported on well since 2004. All equipment at well and tank battery. Owner needs to place well into production or other actions approved by the Chief of Oil & Gas. | ||||
1076097397 | 2004-02-08 | No production for three years ( all equipment present ) pulleys are rusty. New GPS | NONE | |||
1085166216 | 2004-05-23 | Idle well put back into production. RESOLVED. | ||||
1105735673 | 2012-07-12 | Follow-up on Compliance Notice, In-Compliance. | ||||
1317648744 | 2011-09-27 | An inspection of the well revealed no production reported since 2004 and well appears to be idle. All equipment on well and at tank battery, brush growing up around pumping unit and production tanks. No ID at well or tank battery. Plug, produce or place well on temporary inactive status. Submit production records to Columbus Office. Place full and legible ID at well and tank battery. Failure to comply may result in a forfeiture of bond. | 9-1-03C | |||
1317648744 | 2011-09-27 | An inspection of the well revealed no production reported since 2004 and well appears to be idle. All equipment on well and at tank battery, brush growing up around pumping unit and production tanks. No ID at well or tank battery. Plug, produce or place well on temporary inactive status. Submit production records to Columbus Office. Place full and legible ID at well and tank battery. Failure to comply may result in a forfeiture of bond. | 9-9-05(A)10 | |||
1317648744 | 2011-09-27 | An inspection of the well revealed no production reported since 2004 and well appears to be idle. All equipment on well and at tank battery, brush growing up around pumping unit and production tanks. No ID at well or tank battery. Plug, produce or place well on temporary inactive status. Submit production records to Columbus Office. Place full and legible ID at well and tank battery. Failure to comply may result in a forfeiture of bond. | NONE | |||
1317648744 | 2011-09-27 | An inspection of the well revealed no production reported since 2004 and well appears to be idle. All equipment on well and at tank battery, brush growing up around pumping unit and production tanks. No ID at well or tank battery. Plug, produce or place well on temporary inactive status. Submit production records to Columbus Office. Place full and legible ID at well and tank battery. Failure to comply may result in a forfeiture of bond. | NONE_ | |||
1317648744 | 2011-09-27 | An inspection of the well revealed no production reported since 2004 and well appears to be idle. All equipment on well and at tank battery, brush growing up around pumping unit and production tanks. No ID at well or tank battery. Plug, produce or place well on temporary inactive status. Submit production records to Columbus Office. Place full and legible ID at well and tank battery. Failure to comply may result in a forfeiture of bond. | NONEC | |||
1346854152 | 2012-09-05 | MH well service fininshing washing clay, they have rigged down. I have asked the well be left open for two weeks to allow for settlement. | ||||
1840499555 | 2012-08-28 | I received a call from Bruce Kelly, he was servicing this well and could not retrieve all the tubing, Huffman and Bowers on site, they were able to get circulation. I allowed Huffman Bowers to set 250' cement plug on bottom, there are to also set a 200' cement plug from 1700' to 1900', the rest will be clay. | ||||
431082699 | 2012-08-29 | MH well service has removed the 2 3/8 upset tubing, began ripping 4.5 casing at 1890' casing parted at 1650'.I spoke with Pat Shreve concerning the plug job, it was decided to set a 200 cement plug at 1650, then finish clay plugging once the precast plug is set on the 7 seat. | ||||
450289656 | 2012-07-23 | FOLLOW UP TO NOV # 826122208 The inspection revealed well is incapable of producing, according to Bruce Kellie(Owner) the down hole pump is stuck and will need a larger service rig to pull pump. According to landowner company had a service rig on well and was unable to remove stuck pump and removed rig without placing well into production. No production has been reported on well since 2004. All equipment at well and tank battery. Owner needs to place well into production or other actions approved by the Chief of Oil & Gas. | ||||
50130675 | 2012-07-23 | FOLLOW UP TO NOV # 450289656 FOLLOW UP TO NOV # 826122208 The inspection revealed well is incapable of producing, according to Bruce Kellie(Owner) the down hole pump is stuck and will need a larger service rig to pull pump. According to landowner company had a service rig on well and was unable to remove stuck pump and removed rig without placing well into production. No production has been reported on well since 2004. All equipment at well and tank battery. Owner needs to place well into production or other actions approved by the Chief of Oil & Gas. | ||||
681247520 | 2012-08-31 | MH well service clay plugging today, they will start pulling the 8 casing. | ||||
826122208 | 2012-07-23 | The inspection revealed well is incapable of producing, according to Bruce Kellie(Owner) the down hole pump is stuck and will need a larger service rig to pull pump. According to landowner company had a service rig on well and was unable to remove stuck pump and removed rig without placing well into production. No production has been reported on well since 2004. All equipment at well and tank battery. Owner needs to place well into production or other actions approved by the Chief of Oil & Gas. | NONE14 |