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34-099-21452

Well Details

Well ID: 34-099-21452
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1982-07-09
Unconventional:
Horizontal:
Producing: No
Violations: 1
Latitude: 40.938877422
Longitude: -80.9038742113

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1995647708 2005-03-29 The tank battery is shared with permit 1451 and consists of 1-210 bbl storage tank, 1-100 bbl salt water tank a dike and a fence. Permit 1451 has 1-100 bbl storage tank, shared 1-100
1144689759 2006-04-07 Arriveds on site and met with the pumper, Jeremy Kohler, John Bricker Fire Chief, DamascusVFD, Mark DePew Petrox owner and the Jonses. Regarding a explosion and fire. The tank battery was destroyed. The tank battery was shared with permit 1451. Jonses had their truck, boat and horse barn door damaged. Mark will work with them to make restitution. OEPA was notified. Oil got into a stream and traveled approximately 100 yards downstream before being contained. Clean-up crfew on site to effect repairs. Case pends. Photos on M drive Jonnie Patrick Folder. 9-1-07
1682379735 2006-05-11 The contamination has been removed and the tank battery rebuilt. Recommend case be resolved.
438574156 2009-06-23 I walked around the tank battery and the wellhead and found that there were no violations at this time.
PL13193 Preliminary Restoration done information from Data Point