X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-121-21928

Well Details

Well ID: 34-121-21928
Loading map...
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1976-12-02
Unconventional:
Horizontal:
Producing: No
Violations: 4
Latitude: 39.7419839536
Longitude: -81.4632281917

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1342959521 2012-07-19 Inspected site at request of landowner and determined that well is shut in at present time and equipped with 8" surface casing and 4.5" production casing and 1.5" tubing and 1-100 bbl tank and seperator in need of proper dike if placed back into production,all valves were shut at wellhead on the day of my inspection and it is noted that owner has valid plugging permit for said well.

Plug well within 60 days or file for temporary inactive status. Failure to comply may result in bond forfieture.

9-9-02
1342959521 2012-07-19 Inspected site at request of landowner and determined that well is shut in at present time and equipped with 8" surface casing and 4.5" production casing and 1.5" tubing and 1-100 bbl tank and seperator in need of proper dike if placed back into production,all valves were shut at wellhead on the day of my inspection and it is noted that owner has valid plugging permit for said well.

Plug well within 60 days or file for temporary inactive status. Failure to comply may result in bond forfieture.

NONE
1342959521 2012-07-19 Inspected site at request of landowner and determined that well is shut in at present time and equipped with 8" surface casing and 4.5" production casing and 1.5" tubing and 1-100 bbl tank and seperator in need of proper dike if placed back into production,all valves were shut at wellhead on the day of my inspection and it is noted that owner has valid plugging permit for said well.

Plug well within 60 days or file for temporary inactive status. Failure to comply may result in bond forfieture.

NONE_
1342959521 2012-07-19 Inspected site at request of landowner and determined that well is shut in at present time and equipped with 8" surface casing and 4.5" production casing and 1.5" tubing and 1-100 bbl tank and seperator in need of proper dike if placed back into production,all valves were shut at wellhead on the day of my inspection and it is noted that owner has valid plugging permit for said well.

Plug well within 60 days or file for temporary inactive status. Failure to comply may result in bond forfieture.

NONE18
1344527247 2012-07-31 My inspection today finds the casing ripped at 3856'. Chipco set a 30sk plug. The rig was pulling 4.5" casing.
1362506602 2012-07-19 FOLLOW UP TO NOV # 1342959521 Inspected site at request of landowner and determined that well is shut in at present time and equipped with 8" surface casing and 4.5" production casing and 1.5" tubing and 1-100 bbl tank and seperator in need of proper dike if placed back into production,all valves were shut at wellhead on the day of my inspection and it is noted that owner has valid plugging permit for said well.

Plug well within 60 days or file for temporary inactive status. Failure to comply may result in bond forfieture.

1365611068 2013-04-10 follow-up to compliance notice #1342959521 The well has been plugged. The site has been reclaimed to 1509.072 specifications. Vegetation has been established.
1516034557 2012-08-19 Inspection revealed that site has been restored and vegetation has begun to grow.
1775223264 2012-07-25 Inspection revealed that service rig moved in on site to plug said well and they are currently trying to release packer and remove from well so they can properly plug said well.