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34-169-21644

Well Details

Well ID: 34-169-21644
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1971-11-16
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 40.9586801138
Longitude: -81.7898479349

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1664258706 2007-07-15 Arvilla is pulling 5 1/2 inch casing today .
-228483149 2005-10-20 Test M.I.T on well today.and test failed.
-619264944 2007-07-19 Superior Well set wire line at 2210 ft. and then run bond log.
-961668383 2003-12-09 CHECKED ID - OK
1131459575 2005-10-20 Arrive today to conduct an M.I.T. on well # 10-during test it was determined by operator that it would fail and that test should be haulted until problems could be fixed.
1132148765 2005-10-26 Conduct M.I.T for 8 hours and test failed.
1578769641 2008-09-09 There should be a marker installed where well was so it can be found should some reason occur that it needed to be found.
466113158 2006-10-30 Check on plug rig and found that they can not got to bottom with tubing .Can only get to 1900 ft. .
617980501 2006-11-01 Arvilla is still working on junk in the hole at 1950 ft. They are still not sure what is looking up at that depth .
685825987 2007-07-20 Run in with 2/38 tubing and tag plug at 2210 ft. and set plug from 2200 to 1600 ft. and then in stages of 560 ft. to surface .
976661002 2007-07-19 Return to well for pressure test at 500 psi and test passed .