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34-059-24314

Well Details

Well ID: 34-059-24314
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-12-12
Unconventional:
Horizontal:
Producing:
Violations: 0
Latitude: 40.0051860067
Longitude: -81.4112915525

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1899459276 2014-01-09 On the day of my inspection I witnessed that Falcon Rig 23 was rigged down and the 13.375 inch casing was capped. Rig is moving back to Pennsylvania on Monday. Company Man Cliff Heeter said he did not know when the next rig was due on site. Site inspection revealed no violations.
1386944888 2013-12-13 On the day of my inspection, I witnessed cement returns to surface on the 26" conductor casing, there is a air rig mobilizing from Pennsylvania to drill the 20" surface hole.
1387208684 2013-12-16 On the day of my inspection, I witnessed ( Well service Group rig #1 ) drilling at a depth of 450' and to a minimum of 910' so the 20" surface casing can be set in place and cemented back to surface.
1388418572 2013-12-30 On the day of my inspection, I witnessed Falcon Drilling Rig #23 reaming out the bore hole to run the twenty inch surface casing to a depth of nine hundred and twelve foot.
1394723742 2014-03-13 On the day of my inspection, I witnessed Express Energy Service break circulation with fresh water, then displace two hundred and ninety sacks of Class A cement with a weight of 15.6 and a yield of 1.18 at a depth of one hundred and fourteen foot, I witnessed eighteen barrels of cement returns to surface.
1401202868 2014-05-27 On the day of my inspection, I witnessed the Nomac Rig #137 skidding from the 3-H to the permit number above, my site inspection revealed no spills or erosion problems.
1407165420 2014-08-04 On the day of my inspection accompanied by ODNR Intern Austin Gutridge, I witnessed that Schlumberger was on site fracing the said well. Met with AEU Company Man Jude Smith and went over frac schedule and current stage. Schlumberger was on stage 29 of 63. Average treating pressure on stage 29 was 8400psi initially during stage had trouble and had to re-perforate zone.