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34-117-24258

Well Details

Well ID: 34-117-24258
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2014-06-23
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 40.5007982893
Longitude: -82.8204042074

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-125238646 2014-07-10 With Eric Daugstrup. New drilled well. See Eric's report this date for details.
-1396172471 2014-07-02 G & L drilling reached total depth on the intermediate hole at 1500 foot on soap. Ran 35 joints of 17 pound new 7 inch casing with three centralizers and a guide shoe on bottom. Note: ran left handed back off collar at 886'. Formation Cementing hooked up and displaced 81 sacks of 60/40 POZ cement. Plug down 2:45 pm.
-441841245 2014-06-27 G & L Drilling reached total depth on the 12.25 inch surface hole at 374 feet 4:10 am.
-488910043 2014-07-22 Mullins Energy Services has closed the air pit. The lined fluid pit remains for use during plugging operations.
-822759820 2014-08-25 The operator has replaced the top soil and finished grading the entire location.
-842183451 2014-08-06 Appalachian Well Surveys on location. Unable to unscrew 7" swedge or recover the 7" intermediate casing. Decision made to perforate 7" intermediate casing and squeeze. Mr. Kenny Smith cut off swedge and Appalachian ran in hole and perforated the 7" casing at 700' with 4 shots. 2:30pm Formation Cementing hooked up and broke circulation and displaced (bullhead) 92 sacks class A to squeeze cement plug at oil show at 650'(Big Lime). 3:00pm Coshocton Pipe run in hole with tubing for top of surface casing plug. Formation Cementing hooked up and displaced 62 sacks Class A cement from 200 foot to surface which held. Plugging operation co-witnessed by Houghton Investment representative Mr. Bob Atha. **The Howell-Meimer Unit #1 (#4258) is officially plugged and abandoned.
-886831146 2014-07-03 G & L drilling rig #3 shut down for the holiday.
1072330192 2014-06-23 Inspect Mullins Energy services brine truck delivering freshwater for the drilling of the surface hole. UIC and other identification clearly and properly marked. Status: ok.
1188248900 2014-07-18 Received verbal notification of the operators intend to plug and abandon the Howell-Meimer Unit #1 using Coshocton Pipe service rig.
1403117148 2014-06-18 Mullins Energy Services has finished cutting location and stockpiled the topsoil on the south side of the location. G & L drilling has delivered drill collars and drilling mud.
1403182949 2014-06-19 G & L Drilling has delivered additional tubs of equipment and a water tank to the location. Drilling rig scheduled for 6/20/2014.
1403269351 2014-06-20 G & L Drilling has moved its RD-20 drilling rig onto location.
1403530822 2014-06-23 G & L Drilling has begun digging the mud pit and finished rigged up.
1403615223 2014-06-24 G & L Drilling #3 spud the Howell-Meimer Unit #1 with new Varel 12.25" bit at 5:00 am on fresh water mud. 9:30 am drilling ahead at 61'. Fluid pit and cellar completely lined and watertight. Valid drilling permit and conditions properly displayed.
1403708300 2014-06-25 G & L Drilling shut down due to mud pump failure, currently at 189 feet. Waiting on repairs.
1403796285 2014-06-26 Shut down waiting on repairs.
1403881322 2014-06-27 G & L ran 11 joints of new 9.625 inch, 29 pound AT-50 with three centralizers (evenly spaced) and a guide shoe on bottom. 8:00 am Formation Cementing hooked-up and displaced 28.5 barrels of lost circulation material ahead of 190 sacks of class A cement (100% excess) plug down 8:40 am with 6 barrels of returns to surface which held. Formation pressure up casing to 500 pounds with no loss at 5 minutes. Surface casing emplacement and cementing co-witnessed by company representative Mr. Lee Atha.
1404136602 2014-06-30 G & L Drilling currently shut down.
1404315023 2014-07-01 3:15 pm G & L drilling out from surface with 8.875" bit on soap currently at 870 feet. Blow out preventer installed and tested, air pit dug and fully lined.
1404394189 2014-07-02 G&L Drilling rig 3. Witness cement job of 7" casing with Eric Daugstrup. See Eric's reports on details.
1404822980 2014-07-07 G & L Drilling Rig #3 drilling out from intermediate string (7 inch) on air at 1890' (3:00 pm). Blow out preventer (BOP) installed, tested and passed.
1404920142 2014-07-08 G & L Drilling #3 reached total depth at 3420' on air in the Trempealeau. Appalachian wireline logged well. Status: the operator has released G & L Drilling. Plans to plug and/or produce using a service rig.
1405102588 2014-07-11 Location Information for the Howell-Meimer Unit #1 (#4258). ENTRANCE: Lat. 40.49969 Long. -82.81922 / WELL HEAD: Lat. 40.50075 Long. -82.82022 / CENTER-OF-STORAGE: None
1419062512 2014-08-04 Coshocton Pipe service rig has moved onto the location to begin plugging operation under the drilling permit.
1631965940 2014-08-05 Formation Cementing on location to set bottom two plugs through 2.875 inch tubing inside 6.25 inch openhole. Break circulation and pump bottom plug #1 Trempealeau (3380'-3080'), pull tubing and pump plug #2 Trenton (2784'-2634'). Plugs witnessed by Northwest Regional Supervisor Mr. Will Ziegler. Coshocton Pipe lay down tubing and attempt to back off 7" casing at 886'. Unable to back off, shut down for the day.
26172494 2014-08-07 On-site to witness Mr. Kenny Smith (welder) cut the casing off 38 inches below ground and weld the identification tag (ODNR #4258) to the top of surface casing.
635669112 2014-07-15 G & L Drilling rig #3 has rigged down and is parked at the entrance. All drilling related equipment and debris has been removed from location and the site has been rough graded. The mud and air pits are open. Status: will continue to monitor.