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34-121-24382

Well Details

Well ID: 34-121-24382
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2012-11-14
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.745851503
Longitude: -81.4141137237

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-2087232296 2012-11-15 Conductor job they ran 110' of 30" casing and cemented it in place with 520 sacks cement with six barrel of good returns.
-2102955238 2013-11-19 The well site meets the preliminary restoration criteria.
1355772704 2012-12-16 At 7:46 am I received a call from the drilling engineer stating that the blow line had blown apart and some material had escaped containment. Upon arrival I found that while drilling at 426' the blow line had plugged and parted. The driller was using nothing but air at the time. I ask the operator to roll up the straw mulch on the edge of site and replace it since it had cuttings on it.
158643371 2012-11-26 Stopped at the location to check the status of the rig move.
232203772 2012-12-19 On site to witness cementing of 13.375" casing driller ran 1991" of casing and Baker Hughes cemented it in place with 1400 sacks of Class I cement and they ran shoe on bottom and 16 centralize devices.