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34-089-23750

Well Details

Well ID: 34-089-23750
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1981-01-05
Unconventional:
Horizontal:
Producing: No
Violations: 3
Latitude: 39.9767580916
Longitude: -82.2562392928

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1461183975 2011-07-27 I witnessed plugging operations today.
-1690045736 2008-07-08 I witnessed plugging operations today.
-545933662 2011-05-05 Witnessed the pit abandonment at well location with the well owner, Mr. Daryl Porter and cleanup crew.
1304683816 2011-05-05 Witnessed pit abandonment with Brent Bear.
1307363412 2011-05-04 The Division received a complaint from Ohio EPA alleging that a pit containing crude oil has overflowed into a stream. The complainant, Mr. Keith Branski, a caretaker for the property was then contacted. Mr. Branski accompanied me for the inspection. No rainfall at time of the inspection. The well consisted of 4.5" casing with a swage and a valve. The nearby earthen pit was dug exclusively for service work operation performed on the well. The pit contained a liner and measured approx 15' x 5' x 5', but found to have reached it's maximum fluid capacity. An oil sheen was observed on the surface of water however, the pit was not leaking at time of the inspection. Four booms were observed on the right hand side of pit, which have been deployed by the Fire Department per Mr. Branski. The bottom of the pit was sampled, in the field, and High Range Quantabs revealed no Cl-. The area situated below the well location contained an intermittent stream and received drainage/runoff from well location (i.e. lease road). A steady flow of water was observed at time of the inspection. This area was mixed forest located approx 50' - 75' lower in elevation to the pit. No observed impact to both streams. There was no observed crude oil and High Range Quantabs revealed no Cl-. Bacteria/Iron Scales were observed in pooled area around a bend. Mr. Branski was informed there was no observed impact at this time. Prior to Mr. Branski leaving the property, he requested that soil samples be obtained in the stream. Mr. Branski was advised to talk with Ohio EPA. Followed intermittent stream to confluence and again observed no impact to State waters. Note: Well location was not accurate therefore, a GPS reading was obtained during the inspection. A voicemail message was left for the well owner at 1:42 pm and requested a return call. Contacted Mr. Chris Holmes with Ohio EPA and provided the inspection results. Mr. Holmes stated no soil sampling. Provided Mr. Rob Stonerock, West Region Oil & Gas Supervisor, with overview of complaint and inspection results at 1:49 pm. The well owner, Mr. Daryl Porter returned call at 5:06 pm and agreed to remove oil sheen and abandon the pit within 24 hours. Mr. Porter stated both oil and gas wells would be plugged this summer. There was miscommunication with Knox Energy whom serviced this well in November 2010. Further stating they pulled a wet string of 1.5" out of 2.88" tubing consisting of mostly brine and were unable to unseat the pump.
1307629211 2011-05-04 The Division received a complaint alleging idle well. An inspection revealed idle well consisting of 4.5" casing with a swage. Records indicate 2009 production (shared tank battery) with no reported production for 2010. No attached flowline for commercial production or house gas received from this well. No identification observed at the well or tank battery. On 5/5/2011, the well owner stated that well would be plugged this summer. The well owner shall plug or produce this well. If well is placed back into production, identification is required for well and tank battery(shared) locations. The identification shall contain permit number, well name, well number, county, owner name, and emergency contact information. 9-9-05(A)10
1307629211 2011-05-04 The Division received a complaint alleging idle well. An inspection revealed idle well consisting of 4.5" casing with a swage. Records indicate 2009 production (shared tank battery) with no reported production for 2010. No attached flowline for commercial production or house gas received from this well. No identification observed at the well or tank battery. On 5/5/2011, the well owner stated that well would be plugged this summer. The well owner shall plug or produce this well. If well is placed back into production, identification is required for well and tank battery(shared) locations. The identification shall contain permit number, well name, well number, county, owner name, and emergency contact information. NONE
1307629211 2011-05-04 The Division received a complaint alleging idle well. An inspection revealed idle well consisting of 4.5" casing with a swage. Records indicate 2009 production (shared tank battery) with no reported production for 2010. No attached flowline for commercial production or house gas received from this well. No identification observed at the well or tank battery. On 5/5/2011, the well owner stated that well would be plugged this summer. The well owner shall plug or produce this well. If well is placed back into production, identification is required for well and tank battery(shared) locations. The identification shall contain permit number, well name, well number, county, owner name, and emergency contact information. NONE_
138847867 2011-05-06 At 8:45 am, notified the complainant, Mr. Keith Branski, of 5/5/2011 pit abandonment. At 8:49 am, a message was left for Mr. Chris Holmes with Ohio EPA stating pit was abandoned on 5/5/2011.
25103462 2011-07-26 I witnessed plugging operations today.
352750179 2014-08-05 This inspection was conducted as a final restoration status check. The well has been plugged. Equipment has been removed and location restored. Final restoration meets ORC 1509.072 requirements.