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Well ID: 34-117-24137 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1996-09-03 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 6 | |
Latitude: 40.5869820476 | |
Longitude: -82.7675151013 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
-1074311875 | 2014-07-08 | Inspect well for integrity and pressure. | ||||
-1106463957 | 2013-02-20 | Enhanced recovery well status check: Identification posted, well site clean and storage ok. | ||||
-1226153129 | 2014-07-24 | Inspect Mullins Energy Services brine truck on-site for pressure test. Ohio license number PHW-8499. Brine, UIC number and other identification clearly and properly displayed. Status: ok. | ||||
-1253075010 | 2013-02-19 | Conduct line pressure test with air. Pressue line up to 25 psi; the pressure held for 15 minutes. The operaor was given authorization to utilize the well for brine disposal. | ||||
-1334258075 | 2009-02-23 | Chk well and storage, ok. | ||||
-1379860129 | 2013-02-19 | On-site for flow line mechanical integrity test. Passed: Well can be placed into injection. Inspector Benko has details and forms. | ||||
-1474113756 | 2004-08-25 | Follow up on NOV. The well has not been plugged or converted to Enhanced Production. | ||||
-1625203867 | 2011-10-11 | Inspect well. | ||||
-167240608 | 2014-01-17 | Inspected the Logan #1A (ERP #12) as part of a standard injection well status check. Check well, pressures, storage and identification. The operator has added the identification and emergency contact information to the storage. The storage dike is currently ice covered. | ||||
-1807824025 | 2014-04-24 | Inspect well and tank battery. Location is ok. | ||||
-1832569712 | 2007-01-10 | Talked w/Bob Wells (Pumper) and told him he needs to install a quarter inch tap on the annular space so that I can monitor the pressuers on the well. Advised him that I have already issued an NOV to Warpath Energy and that the tap needs to be installed ASAP or I may need to take further leagal action. | ||||
-1833371042 | 2003-07-07 | Follow up on notice issued by Jeff Fry. The well has not been plugged or converted to salt water injection as of this date. I would recommend issuing a Chief's Order. | 9-9-05(A)10 | |||
-1833371042 | 2003-07-07 | Follow up on notice issued by Jeff Fry. The well has not been plugged or converted to salt water injection as of this date. I would recommend issuing a Chief's Order. | NONE | |||
-1896740206 | 2013-02-14 | Inspect re-constructed dike area. Dike are measures 43 feet by 40 feet by 48 inches deep. One(1) new 210 bbl tank has been set on timbers. Identification is taped onto tank. Requested a line test to well head. | ||||
-1924847737 | 2014-08-25 | Inspected the Logan #1A (ERP #4137) as part of a standard injection well status check. Inspect well, pressures, storage and identification. The operator has added a storage shed. Status: ok. | ||||
-1947276178 | 2014-07-24 | Inspected the Logan #1A (ERP #12) as part of a standard injection well status check. Inspect well, pressures, storage, vault and identification. Status: ok. | ||||
-1957961847 | 2012-05-23 | Inspect Well. Pit Liner has failed. Previous repair of line is substandard and inadequate. Fix and replace liner. | ||||
-2028362201 | 2013-12-12 | Inspected the Logan (ERP #12) as part of a standard injection well status check. Check well, pressures, storage and identification. No change in status from previous inspection. The operator has not made corrective actions. | ||||
-209008957 | 2012-10-25 | Inspected the Logan #1 (#4137) (ERP #12) as part of a standard injection well status check. Injection: zero Annulus: 350 psi. Replacement of the dike liner has not occurred. | ||||
-2121696734 | 2012-12-05 | Inspect well for integrity and pressure. There has been no change or reconstruction of dike area as discussed and agreed upon. | ||||
-253493051 | 2010-03-29 | Chk well and storage, ok. | ||||
-370136286 | 2014-01-23 | Location Information. ENTRANCE: Lat. 40.59207 Long. -82.76642 / WELL HEAD: Lat. 40.52150 Long. -82.81357 / CENTER-OF-STORAGE: Lat. 40.58797 Long. -82.76673. | ||||
-380187884 | 2012-06-21 | Preformed a follow up inspection on the Logan (ERP #12) regarding the pit liner as requested by Inspector Tom Benko. Cortland has repaired the liner by relining as an overlay three sides of the dike. The liner has been folder over to create double thickness. The sides relined are the south/west/north sides. The outer edges of the liner are secured by boards and fine limestone. 55% of the new liner is exposed to the elements on the dike walls. The liner is holding fresh rain water as seen by pooling around the tank. Pictures of the liner where sent to Inspector Benko 6/28/2012. | ||||
-426658598 | 2010-05-10 | Chk well and storage ok. | ||||
-456216630 | 2009-06-24 | Ok except that I could not open the valves on the annulus. Need bigger wrench. No fluid in the diked area at this time. | ||||
-603394488 | 2013-11-18 | Inspected the Logan #1 (ERP #12) as part of a standard injection well status check. Check well, pressures, storage and identification. Status: No change in status from previous inspection, contacted operator. | ||||
-641714269 | 2014-07-16 | On-site with UIC inspector Tom Benko as the operator modifies the storage facility according to the approved plan (6/27/2014). Three all fiberglass tanks (210 barrels) have been added as well as a new concrete, fully lined vault. | ||||
-652221388 | 2006-02-23 | Chk well and storage, Ok. | ||||
-75775385 | 2008-09-03 | Chk well and storage, No identification posted. Has positive pressure on annulus but not enough to measure. | ||||
-909557677 | 2012-08-30 | Contacted operator by phone to report that the temporary fixes for the liner were not adequate and that the liner would need to be replaced. | ||||
-962903515 | 2011-05-09 | Need to repair the liner in the diked area it has some holes in it close to the top of the dike. Also need to post identification.
2:00pm called and talked to Bob Masters and told him of the problems. He told me that he would get the liner repaired or replaced and post the identification. |
||||
1036523338 | 2002-11-05 | Service rig removed. Well still has tubing and rods in it. Not capable of production or injection. Operator in past has proposed to convert this well to an injection well. | ||||
1073923234 | 2004-01-12 | Well was to be converted to an injection well. Tubing and rods still in well . Valves closed. No activity.
One digital photo. Need to pursue further enforcement action. |
||||
1095082378 | 2004-09-13 | On site for mechanical integrity test. Ran a new Parmaco HW packer to 3640' pressured up on the annulus would not hold. Shut down for the day. | ||||
1100875720 | 2004-11-19 | Liner put down, and storage tank set. Using well at this time. | ||||
1104262170 | 2004-12-28 | Chk well and storage, Ok. Site is snow covered. Shut down. | ||||
1168008662 | 2007-01-05 | Warpath Energy Inc has done nothing to address the violations. No identification posted, no quarter inch tap on the annulus and the diked area is full of fluid at this time. | ||||
1210i5555520 | 2002-01-31 | Service rig over hole. Part of rods were out. Well is not capable of production.Need to continue with injection well permit . Submit public notice or within 30 days P&A. | ||||
1255023396 | 2009-10-08 | Chk well and storage, Ok. No fluid in diked area at this time. | ||||
1261058906 | 2009-12-17 | Check well and storage, Id posted at the storage site. | ||||
1266305957 | 2005-10-06 | No quarter inch tap on annulus, can not chk annulus pressure. | ||||
1280759002 | 2010-08-02 | Check well and storage, Ok. | ||||
1294079650 | 2011-01-03 | Can not open valve on annulus. Tank has run over at some point and has a small amount of oil in the diked area. | ||||
1297266610 | 2011-02-09 | Check well and storage. Could not open valve on annulus due to the cold weather the valve is frozen. Approx temp 12 degrees F. Need to post new Id. | ||||
1313905919 | 2007-09-27 | Follow up on NOV, Resolved 1/4 inch tap installed on annulus. Ok at this time. | ||||
1345577223 | 2012-08-21 | Inspected the Logan (ERP #12) with Mr. Jeff Fry as part of a standard status check. Backside pressure 375 psi, injection on vacuum. Well identification is displayed at the storage. The dike contains one silver 210 barrel tank in a lined dike. | ||||
1357759326 | 2013-01-09 | Operator began reconstruction of surface facility and removal of tank and old dike liner for replacement dike and liner. New dike area is anticipated to be 30 feet by 30 feet with 48 inch high dike. This construction design will be sufficient to hold two 210 bbl. Tanks. Construction activity included removal of pipe run, emptying tank, removal of tank from dike area, and removal ice and removal of water by vacuum truck. The old pit liner was tore by excavator and was subsequently removed. Construction activity conducted by Ken Pryor. | ||||
1359048681 | 2013-01-24 | The liner replacement has begun. The old liner and tank have been removed and the dike has been rebuilt. Currently waiting on weather to set the liner and tank. | ||||
1359484701 | 2013-01-29 | On site with Inspector Jeff Fry to witness replacement of the dike liner. | ||||
1363129344 | 2014-03-17 | Inspected the Logan #1A (ERP #12) as part of a standard injection well status check. Inspect well, pressures, storage and identification. Status: unable to check pressures, pressure gauge malfunctioning. | ||||
1369711855 | 2014-07-28 | Inspect well and surface facility. The tanks have been placed. The unloading pad has been constructed and the drain is connected to a concrete lined vault. The lines have been pressure tested. Checked the annulus of the well and the pressure is 410 psi. The well is on a strong vacuum. | ||||
1376070267 | 2013-08-09 | Inspected the Logan #1 (#4137/ERP #12) as part of a standard injection well status check. Check well, storage and identification. No change in status from previous inspection, except the dike needs rain water pumped back into the storage. Status: Identification has not been posted (from last inspection 5-23-13), tested dike water: high chloride content contacted operator to evaluate. Will continue to monitor. | ||||
1405686594 | 2014-07-17 | Inspect location. Operator has removed the steel 210 bbl tank and is replacing with three fiberglass tanks. Installed a concrete spray plastic lined vault. | ||||
1405703361 | 2014-07-18 | On-site to witness construction of the concrete unload pad. Canaan Concrete built the forms (rebar reinforced) and Lexington Concrete poured the concrete. Built to plan specs with the addition of curbs parallel to the drain. Photo documented construction. Status: ok. | ||||
1406229478 | 2014-07-24 | On-site accompanied by Inspector Jeff Fry, as a request from the operator for a flow line pressure test. Pressure tested flow line at 110 pounds for 15 minutes with zero loss. Status: passed and the operator is cleared to reconvene operations. | ||||
1406635436 | 2014-07-09 | Inspect surface facility. The existing steel tank has been removed from the dike area in preparation of new tanks. Three 210 bbl fiberglass tanks were delivered to the site for installation. The manufacture is RPX Composites of Commodore, PA. The serial numbers are 200705-13571, 200706-13572, and 200707-13573. | ||||
1489307147 | 2012-10-03 | Replacement of the dike liner has not started as of 10/03/2012. | ||||
1747299995 | 2014-07-18 | Operator has a contractor scheduled to install and construct a new concrete unloading pad. | ||||
1826057688 | 2012-09-10 | Inspected the Logan #1A (ERP #12) as a follow-up for Inspector Tom Benko. Cortland has verbally agreed to replace the entire dike liner. No work has started as of 9/10/2012. | ||||
1844094257 | 2014-04-17 | Change of operator noted: George Woodcock dba West Drilling. New identification and emergency contact information has been posted. | ||||
191892232 | 2010-09-22 | Check well and storage, tank appears to have run over at some time. Need to post Id. | ||||
1959975824 | 2013-05-23 | The well has been converted to ERP. Preliminary restoration complete. | ||||
2059832166 | 2014-07-28 | Inspect Mullins Energy Services Truck #3 UIC 25-538. Collect Brine sample from truck at unloading pad. Brine source is 3411722340 The Hohl #1. | ||||
2086455480 | 2005-06-08 | Chk well and storage, Ok. Did not chk annulus no quarter inch tap. | ||||
240384081 | 2013-05-23 | Inspect enhanced recovery well, storage and identification. Status: identification needs posted at storage and well, contacted operator. | ||||
277846138 | 2006-09-29 | Chk well and storage, diked area has fluid in it and needs to be empied. No identification, no quarter inch tap for annualr space. | 9-5-09(A)(3) | |||
277846138 | 2006-09-29 | Chk well and storage, diked area has fluid in it and needs to be empied. No identification, no quarter inch tap for annualr space. | NONE(H) | |||
383014237 | 2008-03-06 | Wwell head is ice covered. Dyke is full of fluid and forzen. | ||||
406070744 | 2014-07-24 | Inspector Eric Daugstrup and myself witnessed an injection line test for Tom Benko. Test passed with no loss. We met new well owner George Woodcock. See Eric's report for this date on details. | ||||
464733866 | 2007-05-16 | No quarter inch tap on annulus. | ||||
481640901 | 2007-10-31 | Chk well and storage, Ok. | ||||
692892257 | 2008-12-11 | Chk well and storage, Ok. | ||||
860449212 | 2013-02-14 | Cortland is preparing to put the well back into injection. Pressure testing of the flow line is schedule for 2/19/2013. | ||||
880782253 | 2005-12-14 | Chk well and storage,ok. | ||||
96023023 | 2013-09-30 | Inspected the Logan #1A (ERP #12) as part of a standard injection well status check. Check well, storage and identification. No change in status from previous inspection: the identification and emergency contact information is not posted and the dike needs emptied of excess water. Status: contacted operator . Will continue to monitor. | ||||
970721939 | 2012-02-23 | Inspect Well. | ||||
9966979 | 2014-07-21 | Inspect well location. Concrete unloading pad has been poured and is in place. Drain vault is in place and has been buried. Three fiberglass tanks have been set and piping has been installed. | ||||
CENT2172 | 1997-10-20 | 1501:9-1-07 | 9-1-07 | |||
CENT2174 | 1997-10-20 | 1501:9-9-05 | 9-9-05(A)10 |