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Well ID: 34-067-21112 | Loading map...
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Spud Date: 2013-03-20 | |
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Producing: No | |
Violations: 0 | |
Latitude: 40.3536548889 | |
Longitude: -81.1080129826 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1787260773 | 2013-09-26 | On the Day of my inspection the site passed preliminary restoration according to 1509.072A. | ||||
1363825351 | 2013-03-20 | I am on site today to witness the running and the cementing of the 13-3/8'inch diameter casing string. Nomac Drilling Rig # 71 drilled a 17-5/8' diameter hole to 615 ft and ran 602 ft of casing. Baker Hughes Cementing Service c/w 556 sks of class A cement . During the inspection it was determined that they would not get casing to bottom for several hours. Returned that evening after contacting Uniontown to advise and witnessed cement circulate to surface. After cement was displaced and the plug was landed the cement head blew off at 550 P.S.I. The floats held and no cement flowed. No one was on the floor at that time so nobody was hurt. | ||||
902335375 | 2012-11-08 | Arrived on location for cementing of conductor pipe, set 20 pipe at 120' with 226 sacks. |