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34-163-20445

Well Details

Well ID: 34-163-20445
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1980-08-14
Unconventional:
Horizontal:
Producing: No
Violations: 3
Latitude: 39.3373469182
Longitude: -82.4599263324

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1269i159 2001-04-10 Follow - up on NOV , In - Complaince
1269i65 2001-02-27 An inspection of the well site revealed that the ID at the well site needs rewrote , may want to bring new ID sticker . 9-9-05(A)10
210839774 2013-11-18 Compliance notice follow up, the well is in compliance from notice written 04/10/2001.
29074183 2013-11-18 There has been no production shown to the division since 2005. All the valves are closed, the polish rod is dull and there are no belts on the unit. I spoke with Doug Adams on 11/18/13 at 1231 hours. He stated he did not own the well but it is still under his bond. I informed Doug Adams as long as the well was under his bond it would be his responsible to bring the well into compliance. The well needs to be brought back into production or plugged in accordance 1509. Annual production reports need to filed with the division . Adams Oil and Gas has until 01/28/14 to bring the well into compliance. NONE_
29074183 2013-11-18 There has been no production shown to the division since 2005. All the valves are closed, the polish rod is dull and there are no belts on the unit. I spoke with Doug Adams on 11/18/13 at 1231 hours. He stated he did not own the well but it is still under his bond. I informed Doug Adams as long as the well was under his bond it would be his responsible to bring the well into compliance. The well needs to be brought back into production or plugged in accordance 1509. Annual production reports need to filed with the division . Adams Oil and Gas has until 01/28/14 to bring the well into compliance. NONEC