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34-121-24418

Well Details

Well ID: 34-121-24418
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-05-18
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.8377751442
Longitude: -81.3930559638

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1272997038 2013-07-22 My inspection today finds the rig crew is running 7150' of 9.625" casing.
-1665470305 2013-07-12 My inspection today finds the operator is drilling the 12.25" section of the well at a depth of 2433'
-417719886 2013-05-30 My inspection today finds Enviro-spud has drilled to a depth of 249'. The rig is currently broke down.
-912656021 2013-07-23 I am onsite to witness the cementing of the first stage of the 9.625" casing. Calfrac circulated 978 sks of 15.5# cement into place.
1102375915 2013-07-01 My inspection today finds the drilling rig (Savanna 640) is making up their bottom hole assembly and preparing to drill the 17.5" section of the well.
1239415253 2013-07-08 The drilling rig is currently hooking up equipment to pressure test the 13.375" casing string.
1370167318 2013-06-01 My inspection today finds the drilling contractor Eviro-spud is ran 309' of 20" casing. Calfrac cemented the casing in place with class A cement. 20 bbl of cement returns to surface.
1374776608 2013-07-17 My inspection today finds the drilling rig has shut down due to the top drive being broken. Current depth is 5088'.
1375297606 2013-07-25 I received a call from CNX stating that they had a diesel spill on location. Upon my arrival the spill was 95% cleaned. The estimated total of the spill was 56 gallons with 50 gallons being held on the primary containment. All material off of containment that was impacted was hauled off to a disposal facility.
1417801255 2013-07-23 I am onsite to witness the second stage cementing of the 9.625" casing The stage tool is set at 4262'. Calfrac circulated 882 sks of 13.8# cement into place. I witnessed 30 bbl of cement returns to surface.
277319173 2013-06-08 Redstone drilling ran casing to a depth of 313'. Calfrac circulated 629 sks of class a cement. There were no cement returns to surface. Weatherford will bond log the well to find cement top.