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Well ID: 34-073-21949 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1982-10-18 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 12 | |
Latitude: 39.5016255884 | |
Longitude: -82.3428111451 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
-1168001730 | 2008-04-21 | A follow-up inspection revealed that the company is working towards resolving FR. | ||||
-1257278333 | 2005-10-26 | No violations, storage tanks have been removed, using production tanks on hill. | ||||
-126573055 | 2003-03-04 | Follow-up on NOV, In-Compliance | ||||
-1504835184 | 2005-03-03 | No violations. | ||||
-193956336 | 2005-06-09 | FOLLOW UP TO NOV # 1246192697 An inspection of the well revealed oil and water in dike around storage tanks, it appears that a storage tank may be leaking. | 9-9-05(A)8 | |||
-322820453 | 2005-04-06 | No violations. | ||||
-386568954 | 2003-01-29 | An inspection of the well revealed that the ID at the well and tanks is not legible, and water in dike around brine tank needs pumped out and need pressure on the annular side of well. REWRITE THE ID, PUMP OUT WATER, AND PRESSURE ANNULAR SIDE OF WELL | 9-5-10(F) | |||
-386568954 | 2003-01-29 | An inspection of the well revealed that the ID at the well and tanks is not legible, and water in dike around brine tank needs pumped out and need pressure on the annular side of well. REWRITE THE ID, PUMP OUT WATER, AND PRESSURE ANNULAR SIDE OF WELL | NONE(H) | |||
-396207331 | 2004-02-26 | No violations. | ||||
-781700336 | 2004-01-27 | No violations. | ||||
-861585887 | 2006-10-06 | Violations have not been resolved. | ||||
-974091041 | 2006-07-13 | An inspection was conducted at the facility owned by Knox Energy Inc. on 7/13/2006. During the inspection, it was noted that there was no pressure at the injection or annulus sides of the well. A mini test will be required. On 7/19/2006, Mr. Dave Harris was informed of the deficiencies found during the inspection. | 9-5-10(F) | |||
1111207241 | 2004-08-19 | An inspection of the well revealed for the past several months no pressure on injection or annulus side of well. Well has have a Mini test done. NEW LAT & LONG | 9-5-09 C | |||
1246192697 | 2005-06-09 | An inspection of the well revealed oil and water in dike around storage tanks, it appears that a storage tank may be leaking. | 9-9-05(A)8 | |||
1269i514 | 2001-11-13 | An inspection of the well revealed that brine in the dike around the tanks, and was unable to check the pressures on the well. The 1/4" valve on the injection side needs replaced, and the 2" valve on the annulus side was closed unable to check pressure. | 9-5-06 | |||
1269i514 | 2001-11-13 | An inspection of the well revealed that brine in the dike around the tanks, and was unable to check the pressures on the well. The 1/4" valve on the injection side needs replaced, and the 2" valve on the annulus side was closed unable to check pressure. | 9-5-09(A)(3) | |||
1269i514 | 2001-11-13 | An inspection of the well revealed that brine in the dike around the tanks, and was unable to check the pressures on the well. The 1/4" valve on the injection side needs replaced, and the 2" valve on the annulus side was closed unable to check pressure. | 9-5-09(B)7 | |||
1269i699 | 2002-01-16 | No violations. | ||||
1269i876 | 2002-03-19 | No violations. | ||||
1269i952 | 2002-04-05 | Follow-up on NOV, In-Compliance, done a MIT test on well and well passed test. | ||||
1273911706 | 2004-05-27 | No violations. | ||||
1309772722 | 2007-11-19 | An inspection revealed that the final restoration does not meet requirements. Steel pipe was observed alongside the lease road. | NONEA | |||
1907444339 | 2004-09-24 | In-Compliance | ||||
1931152432 | 2003-10-27 | No violations. | ||||
1956243145 | 2003-06-19 | No violations. | ||||
2128308757 | 2007-03-20 | On 3/20/2007, this well was plugged by Berry Well Service. The previously noted violation has been resolved. | ||||
227364717 | 2003-12-09 | No violations. | ||||
311357203 | 2004-04-01 | No violations. | ||||
315277806 | 2004-12-14 | No violations. | ||||
34680978 | 2008-05-30 | A follow-up inspection revealed that the final restoration meets requirements. | ||||
492694112 | 2006-11-20 | A mini- test was performed on 11/20/2006. During the test, it was noted that the well was not holding pressure. Mr. Tom Tomastik was contacted and informed of the test results. A Chiefs Order will be issued requiring Knox Energy to suspend injection. | ||||
556078490 | 2003-05-06 | No violations. | ||||
5609i212 | 2001-06-04 | An inspection of the well revealed no pressure on the injection side or the annulus side, it appears it has been some time since the well has been mantained and tested. Request that the Company notify the Beverly Office and set up a date and time for testing packer(mini test). | 9-5-10(E) | |||
5609i212 | 2001-06-04 | An inspection of the well revealed no pressure on the injection side or the annulus side, it appears it has been some time since the well has been mantained and tested. Request that the Company notify the Beverly Office and set up a date and time for testing packer(mini test). | 9-5-10(G) | |||
980662067 | 2003-07-24 | No violations. | ||||
PL16358 | Preliminary Restoration done information from Data Point | |||||
UIC462 | 1987-09-28 | 1501:9-3-06 (H) | ||||
UIC463 | 1987-09-28 | 1501:9-5-09 (B)(7) | ||||
UIC516 | 1988-04-05 | 1501:9-5-09 (A)(6) | ||||
UIC76 | 1986-12-29 | 1501:9-5-06 | ||||
UIC77 | 1986-12-29 | 1501:9-5-09(A)(6) | ||||
UIC934 | 1990-06-18 | 1509.22 (A) (1) | ||||
UIC935 | 1990-06-18 | 1509: 9-5-06 PREVENT OF CONTAMIN | ||||
UIC936 | 1990-06-18 | 1501:9-5-09 (A) (6) CONSTRUCT & CONVERS. |