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34-127-20965

Well Details

Well ID: 34-127-20965
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1947-06-12
Unconventional:
Horizontal:
Producing: No
Violations: 3
Latitude: 39.8202611863
Longitude: -82.1883365076

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1682691911 2014-06-02 I returned to this well to do a follow-up inspection on the well. It appears the company has had someone in here working on the well. The old standing derrick that was here is gone. They have removed all the old wood away from the well and had a dozer clean out the location. The flow line is hooked up to the wellhead but there is still no pumping unit. I called Danny Baker and left him a message to call me about the well.
-392853840 2007-11-19 No violations.
-664145960 2014-02-25 I did a follow-up on this well. The old standing derrick that was around the well has been torn down. There has been some work done around the well site. The pumping unit is still not on the well and the well appears not to be production yet. The compliance date for the violation is 7/7/2014. I will e-mail Jeanie Enterprises to see if they plan on putting the well back in production.
1219674842 2008-08-20 No violations.
1256665430 2009-10-13 AN inspection of the tank battery revealed a production tanks has a hole in the heater tube which allowed approx 60 bbls of oil to flow into dike and near by creek. Approx. 2 bbls entered creek and traveled approx. 2500'ft down stream. Company is cleaning spill up and has removed the leaking tank. 9-1-07
1256665430 2009-10-13 AN inspection of the tank battery revealed a production tanks has a hole in the heater tube which allowed approx 60 bbls of oil to flow into dike and near by creek. Approx. 2 bbls entered creek and traveled approx. 2500'ft down stream. Company is cleaning spill up and has removed the leaking tank. 9-9-05(A)9
1256766769 2009-10-15 Checked clean up on oil spill, appears most of the oil has been cleaned up and removed from creek area, will have company leave booms and pads in creek for a few days.
1829250032 2011-11-01 No violations at this time.
1865707870 2013-12-30 During the inspection of this well I found the pumping unit has been pulled off of the well. The production valves are shut in on the wellhead making it incapable of production. The well will need to be put back in production within 90days or plugging is required within 180days. NONE_