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34-121-24437

Well Details

Well ID: 34-121-24437
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-08-29
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.9136024266
Longitude: -81.3144748534

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-2142052963 2013-11-07 My inspection today finds the drilling rig is drilling 17.5" hole at a depth of 1610'. A visual inspection of the primary containment found no holes or leaks.
151756202 2013-08-29 Express drilled a 30 inch hole to a depth of 100' and ran 100' of 26" conductor. Allied cemented it in place with 336 sks of class A cement. Good returns to surface.
2056573928 2013-11-20 The rig, Patterson 342, is drilling ahead in the 8.5" section of the well at a depth of 8658'.
4943619 2014-04-30 My inspection finds the diesel spill that took place during the completion phase is still causing some sheen on top of the water in the sump. The company is hauling all water off site to be disposed of or recycled. I have asked the company to remove all contaminated stone and soil. The tank battery is comprised of eight 400 bbl tanks set in a containment system.
52810328 2013-11-05 My inspection today finds the rig ran 18.625" to a depth of 381'. Allied cemented the casing in place with 722 sks of class A cement.