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Well ID: 34-111-24288 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2013-11-28 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 0 | |
Latitude: 39.6977567849 | |
Longitude: -80.8987951255 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1087881794 | 2013-11-18 | The said well was spudded by on 11/15/2013 by Butche's Rat Hole with 100' of 20 conductor being set and cemented to surface, A 20 diameter mouse hole is being drilled with a 16 pipe to be set and cemented by grouting to surface with a .500 thick steel plate on bottom. | ||||
-514829846 | 2014-04-07 | Status check inspection on the recent plug back of the 6.250 production borehole due to the company not being able to maintain the required build rate with the 6.250 directional assembly and 4 drill pipe. On 04/05/14 a total of 4 plugs were set through 100' of 2.875 tubing under the drill pipe from 6154' to 2477' in 4- 900' increments with the plug being tagged at 2540', the well bore drilling was the resumed using a 8.5 directional drilling assembly with a current drilling depth of 4232'. | ||||
1395932094 | 2014-03-27 | Status check inspection on the drilling process found the 9.625 casing has been set to a depth of 2750' and the company has drilled out from under the casing to begin drilling the 6.125 production well bore, a formation integrity test was conducted using 8.4# mud by increasing the annular pressure to 1050 psi giving a formation integrity equal to 15.8# mud. | ||||
1397524793 | 2014-04-14 | Status check inspection on the drilling progress found the 8.5 production borehole has been drilled to a depth of 13,255' at a azimuth of 135 degrees, the well has had 20# casing ran with a float shoe and collar along with a rapid start valve used and proper centralizer placement demonstrated, Halliburton cement services has finished cementing the production casing in place with a calculated top of cement at 1,467'. | ||||
1405373520 | 2014-07-12 | On site along with Deputy Chief Bob Worstall to witness Halliburton pump kill fluid into well at 3000 psi and pressure started to drop and pump rate was increased and after pumping 135 bbl of fluid well was static and on slight vacuum and decision was made to rig up onto the next well. | ||||
1405426705 | 2014-07-14 | Status check follow up to the recent location fire. On this day the said well had the well completion control head and piping removed and Horizontal wireline service set a 10,000 psi rated retrievable bridge plug at a depth of 5,000'. Inspection of the North East corner of the well pad working area observed some chemicals released during the fire were still migrating to the corner of the location and notification was made to Stat oil's company men on site and a 3rd party contractor was utilized to recover the product with a morning report on 07/15/14 from the vacuum truck operator indicating he recovered approximately 40 barrels of product. My observation and inspection of the plastic underlying containment has found the plastic containment primarily still intact in the North East corner and retaining fluid allowing for the recovery of the released product. | ||||
1405541324 | 2014-07-16 | Status check on site inspection to witness the changing out of the well tubing head and master control valve, a backpressure valve was set in the well head assembly on 07/15/2014 giving 3 levels of well bore protection to allow the well head assemblies to be changed out, the assemblies were pressure tested to 5,000 psi. Wells number 5-6&7 were in process of being stimulated on 06/28/2014 when a equipment fire broke out on location causing the chain of events leading the wellheads to be changed for structural integrity reasons. | ||||
2098287310 | 2013-12-26 | On 12/26/13 Orion drilling is now rigged up on the hole and 483' of 13.375 surface casing was ran and cemented to surface by Halliburton cement service with 15 barrels of cement returns to surface and a sting in cement collar ran. | ||||
68718152 | 2014-04-02 | Status check inspection of the work over process found the current drilling depth to be 6,164' using a 6.250 direction drilling assembly, the company is unable to get their required build rate of 30 degrees and has requested permission to plug the well back to the vertical section and re-drill the borehole using a 8.5 diameter drill, permission was granted to make the changes needed. |