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34-081-61058

Well Details

Well ID: 34-081-61058
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 40.5053949926
Longitude: -80.6887302648

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1380495823 2013-09-25 We pulled 1362' of 2" tubing and 1095' of 1" tubing from the gas escape packer which was set at 1095'. We ran a 125 sack first cement plug and will log the hole tomorrow to determine what can be done with the 6 5/8" casing/
1866939236 2013-09-26 I was onsite to witness Appalachian well services log the 6 5/8" casing. We found 450' of free pipe but decided to shoot it off at 250' and pull the casing. The cement was tagged at 649' from the previous first cement stage. We were able to pull 250' of 6 5/8" casing and ran into the hole with 595' of 2 3/8" tubing to set the final cement plug. The well circulated and the plug was brought to surface.
1944144021 2013-09-27 Checked the cement level of the last plug. Cement fell 27' and will be topped off when 61059 is cemented the start of next week.