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| Well ID: 34-029-21847 | Loading map...
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| First Permit Date: | |
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| Spud Date: 2014-05-09 | |
| Unconventional: | |
| Horizontal: | |
| Producing: No | |
| Violations: 0 | |
| Latitude: 40.7454443612 | |
| Longitude: -80.9404131843 |
| PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
|---|
| PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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| INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
|---|---|---|---|---|---|---|
| -2135620601 | 2014-05-24 | Nomac Rig 70 drilled a 17.5" hole 559.56' and ran 556' of 13 3/8 J-55 surface casing. O-Tex Pumping was on location to cement the surface casing. After the safety meeting they pressured tested there lines. They pumped 30 barrels of gel, followed by 10 barrels of fresh water, followed by 109 barrels of 15.6# weight of Premium H 2% CaCl2, o.4%1P, 1/4lb/sk Cello Flake. Displaced with 65 barrels of fresh water. Plug landed and held. There was 20 barrels of cement to surface. | ||||
| 1342144857 | 2014-06-10 | Nomac Rig 70 drilled a 8.750' hole to a total depth of 20540'. At present there are laying down drill pipe getting ready to run the 5.5" production casing. They will give me a call when ready to cement the production casing. | ||||
| 1406562128 | 2014-05-20 | I meet with Wade ( Chesapeake Company Man ) and gave him my phone number and told him that I would be the contact person to call when they were getting ready to cement there casing strings. The drilling permit is posted. | ||||
| 1817157414 | 2014-06-05 | I performed a status check on the above location. Nomac Rig 70 is currently drilling at a depth of 13300'. Permit and conditions are posted in the company house. There were no noted violations at this time. | ||||
| 2014995687 | 2014-06-12 | Nomac Rig 70 drilled a 8.750' hole to a total depth of 20540'. They ran 20517' of P110HC 20# 5.5" production casing. Nomac Rig 70 circulated the hole after landing the production casing. O-Tex Pumping 50 barrels of Barite followed by 660 sacks of Lead 50/50 POZ 10% NaCl (BWOW), 0.6% C41P 11.5 # cement. This was followed by 2750 sacks of Premium H 5% KCI (BWOW), 0.6% C-12, 0.4% C-51, 0.1% C-5, 0.05% C-2015.3# Tail cement. Displaced with 450 barrels of fresh water. Floats held 3.5 barrels back in the in tub. Job completed. I only witness the lead cement. |