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Well ID: 34-149-20127 | Loading map...
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Operator Name: | |
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First Permit Date: | |
Last Permit Date: | |
Spud Date: 1990-09-05 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 1 | |
Latitude: 40.3006705829 | |
Longitude: -84.2208213827 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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1145364493 | 2006-04-11 | -On site for status check and to take photos of the well. Had planned to go to the Wenrick well # 20057 but looked at this well instead of the Wenrick well on Cisco Road. Did not have to file during inspection to check the location. Valves off on the gas well. Well not ID'ed. Met with John Firko of Power Gas Marketing on 3/22/04. Well has since been transferred from EDC to Power Gas Marketing. Also met at the well with Bob Huwer. At that time, Firko was going to see where the gas line ran and see if he could put it into production. If not, he was going to have Huwer plug the well. N.O.V. # 383210044 issued 3/22/04 for lack of well identification. | ||||
1196716842 | 2007-11-29 | -Canclled N.O.V. # 383210044 issued 4/01/04 for produce or plug the well and the well not identified.
-Temple Oil and Gas contracted by well owner Power Gas Marketing-North Coast Energy to plug the well. 42 feet of 10' surface casing and 290' of 7 inch casing left in hole (excluding 30 inches cut off below surface. No production tubing. Tremie pipe used to pump cement for cement plugs. Class A cement used with 4% bentonite gel additive. First plug from 1283-1059. Second plug from 390-190. Third plug from 100 feet to 30 inches below the surface. 33 sacks, 30, & 20 sacks in bottom, middle, & upper plug each. Freshwater was used as spacer. 16 bbls between bottom & middle plug and 8 bbls between middle & upper plug. Pit was dug but not needed. No fluids circulated. Casing to be cut off, cap placed, hole covered, and pit filled back in. Will do final restoration inspection on 12/4/07. |
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1196866555 | 2007-12-04 | -On site for final restoration inspection. Joint inspection with Jeff Fry. Well was plugged on 11/29/07. After well was cemented, the 10" and 7" surface casing was cut off about 30" below the surface, the cap w/ ID was placed over the well and well filled back in. The pit dug for any excess fluid was filled back in and graded after the 11/29/07 inspection. Both the pit area and well area was seeded and hay used as mulch for cover. All production equipment has been removed. N.O.V. # 383210044 was issued on 4/01/04 for the well which was incapable of production and not identified. N.O.V. was terminated on 11/29/07. Final restoration has passed. Signed plugging report form later in the day for Dana Blue of Temple Oil. | ||||
383210044 | 2004-03-22 | -On site for status check and meeting with John Firko of Power Gas Marketing (acquired EDC's wells in the mid-1990's. Also met with Bob Huwer of Huwer Drilling. Well permit approved 8/30/90; well spudded 9/5/90; Total depth reached 9/6/90; well completion report dated 9/24/90. Total depth of this Trenton Limestone well is 1280' (drillers) & 1284' (loggers). 10" conductor casing set to 64 feet. 8.62" surface casing to 302 feet. Last reported gas production was in 1991. Sign on well not legible. Valve turned off. Some gas pressure when valve opened. Do not know where the gas line runs. John Firko to find out. Roots meter valve split. Fisher regulator (25-60psi). Firko to check feasibility of putting well into production. If not, will have Huwer plug. | 9-9-05(A)10 | |||
PL5645 | Preliminary Restoration done information from Data Point |