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34-099-22472

Well Details

Well ID: 34-099-22472
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1991-05-10
Unconventional:
Horizontal:
Producing: No
Violations: 6
Latitude: 40.9686248632
Longitude: -80.8863139445

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-155804773 2003-10-22 Meets requirements.
-1918460864 2003-10-22 NONE
-57138573 2007-09-04 I received an anonymous letter in the mail about a well that has been inactive for quit a few years. I inspected the well site, took pictures and GPS'd it. The well is in the northeast corner of the Goshen Township park. There is no production records in the Columbus office. Please send me your production records on this well for the first 6 months of 2007 and all of 2006. This well needs to be either put into production or plugged. I called Mike Murnane from Columbus Oilfield Expl. Co. 614-848-9705. He stated that he would file for TA status. I told him that I would call next Monday, Sept. 11 to see whether he had filed for the TA status yet. 9-9-02
-57138573 2007-09-04 I received an anonymous letter in the mail about a well that has been inactive for quit a few years. I inspected the well site, took pictures and GPS'd it. The well is in the northeast corner of the Goshen Township park. There is no production records in the Columbus office. Please send me your production records on this well for the first 6 months of 2007 and all of 2006. This well needs to be either put into production or plugged. I called Mike Murnane from Columbus Oilfield Expl. Co. 614-848-9705. He stated that he would file for TA status. I told him that I would call next Monday, Sept. 11 to see whether he had filed for the TA status yet. 9-9-05(A)1
-57138573 2007-09-04 I received an anonymous letter in the mail about a well that has been inactive for quit a few years. I inspected the well site, took pictures and GPS'd it. The well is in the northeast corner of the Goshen Township park. There is no production records in the Columbus office. Please send me your production records on this well for the first 6 months of 2007 and all of 2006. This well needs to be either put into production or plugged. I called Mike Murnane from Columbus Oilfield Expl. Co. 614-848-9705. He stated that he would file for TA status. I told him that I would call next Monday, Sept. 11 to see whether he had filed for the TA status yet. 9-9-05(A)10
-728975825 2009-02-18 I performed a field inspection per request from Jay Cheslock. I downloaded the GPS coordinates from the 3D Topo map. I then made a visual inspection of the area. I inspected the area 50 feet around the GPS coordinates. This well was in the Bricker Homstead Walking Park, northeast corner and was plugged with final restoration in 4/08. There were no signs of a well. There were no violations at this time.
1189594032 2007-09-10 I called Mr. Mike Mornane about TA'd status. He said that he had not file TA'd status yet. But will do so. I told him to call me when he had filed. Case continues.
1202736217 2008-02-08 I received a call from Mr. Mike Murnane of Columbus Oilfield Exp.(614-848-9705). Everything was ready to go. But the roads are posted to 13 tons only. The Mahoning County frost laws are in effect until May. So we wait. I inspected the well and made sure the road around the site were posted. All the area roads are posted. We wait. Case continues
1209403699 2008-04-28 I witnessed the 8 5/8" and 5 1/2" casing being cut off and a plate with the API number welded on. The location was dressed up. Rain caused some mud. Will finish up when dryer. NO gas was coming up casing. There were no violations at this time. This case is resolved except for final restoration.
1216i153 2002-01-16 Well inspected at the request of Columbus, Tom Tugend. Well remains idle. NONE
1216i969 2002-10-18 Company has failed to plug or produce the well. NONE
1696206136 2008-07-08 I performed a final restoration status check. The pits were closed and the casing cut off 4' below ground level. Production equipment is gone. Vegetation is growing. There was never a tank battery or a production line. This well PASSES FINAL RESTORATION.
684462018 2008-04-25 I witnessed the plugging of the 5 1/2" casing. The digging up and cutting off of the casing will be done 4/28/08. There were no violations at this time. Case continues.
70277568 2002-07-24 Well remains idle and incapable of production. It is requested that a Chief's Order be issued to plug or produce.