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34-117-23071

Well Details

Well ID: 34-117-23071
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1968-08-07
Unconventional:
Horizontal:
Producing: No
Violations: 1
Latitude: 40.4517150925
Longitude: -82.735152261

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1022332610 2014-07-01 Inspected the Charles #2 (#3071) as part of a standard final restoration status check. Well casing has been buried and erosion control established (in woods). All visual evidence of production equipment has been removed. Remaining lease road and storage is currently being utilized by the Charles #1 (#3091). Status: final restoration complete.
-117741501 2006-01-11 Chk well and storage, Ok.
115312021 2010-01-04 Check well and storage. The site is snow covered. No problems to note at this time.
1341508901 2012-07-05 Inspected the Charles #2 (#3071) as part of a standard status check. No production has been reported to the state since 2006. The pump jack has been removed from the well and the well sits with the rods protruding from the wellhead. The well is incapable of production and needs to be plugged or placed back into production. NONE_
1348575613 2012-09-25 Omega cementing on location to plug the Charles #2 (#3071) using Fishburn service rig. 9:00 am Omega hook-up and break circulation and set bottom hole plug (3688'-3288') through tubing. 9:30 am Fishburn begin pulling tubing. 11:30 am trying to find a telegraph. 2:00pm having trouble finding telegraph moving up hole one joint at a time. 3:15 finally rip pipe at 864'. Lay down 4.5" casing.
1348842160 2012-09-26 Omega hook-up and finish plugging well, circulated cement to surface on last plug which held. This satisfies the corrective notice for non-production written 7/19/2012.
1349358145 2012-10-04 Inspect for cement top. Held within specifications.
793760058 2008-04-04 Chk well and storage, Ok.