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34-153-21025

Well Details

Well ID: 34-153-21025
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1981-10-30
Unconventional:
Horizontal:
Producing: No
Violations: 10
Latitude: 41.0206774391
Longitude: -81.6175671602

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1044533484 2004-07-20 The equipment is deteriorating and leaking. The well must be plugged and abandoned as soon as possible. 9-9-05(A)10
-1044533484 2004-07-20 The equipment is deteriorating and leaking. The well must be plugged and abandoned as soon as possible. 9-9-05(A)9
-1418511021 2003-10-09 The well is still under order to plug and abandon or produce. The problem has been the possible influence of the PPG solution mining operation. Inspected the site with Tom Tomastik for his input on how to plug and abandon the well. 9-9-05(A)10
-1418511021 2003-10-09 The well is still under order to plug and abandon or produce. The problem has been the possible influence of the PPG solution mining operation. Inspected the site with Tom Tomastik for his input on how to plug and abandon the well. 9-9-05(A)9
-1451730535 2005-08-17 The site has been rough graded with stock tanks still on site.
-1598034840 2002-05-23 FOLLOW UP TO NOV # 87 Random status check. Operator has never reported production and according to facility employees, the well has not been in production for at least eight years. Well is equipped with one 210 bbl stock tank, one 60 bbl brine tank, one horizontal separator, 9-9-05(A)10
-1598034840 2002-05-23 FOLLOW UP TO NOV # 87 Random status check. Operator has never reported production and according to facility employees, the well has not been in production for at least eight years. Well is equipped with one 210 bbl stock tank, one 60 bbl brine tank, one horizontal separator, 9-9-05(A)9
-1611384798 2003-01-31 The requested signage and retention dike have not been installed. The well is located due west of Wolf Creek with a reasonable likelihood of any uncontained spill impacting the creek. The well still provides a small amount of gas to the B&C facility and is therefore not considered idle. Contacted Dan Cook (330-753-5081) with B&C regarding the violations and am waiting for a response. 9-9-05(A)10
-1611384798 2003-01-31 The requested signage and retention dike have not been installed. The well is located due west of Wolf Creek with a reasonable likelihood of any uncontained spill impacting the creek. The well still provides a small amount of gas to the B&C facility and is therefore not considered idle. Contacted Dan Cook (330-753-5081) with B&C regarding the violations and am waiting for a response. 9-9-05(A)9
-2140944103 2005-08-15 The well has been plugged and abandoned and the violation has been corrected. 9-9-05(A)10
-2140944103 2005-08-15 The well has been plugged and abandoned and the violation has been corrected. 9-9-05(A)9
-937391432 2005-08-03 Met on site with Steve Hagen (Intrepid Well Service) to determine annular flow from this well prior to plugging. The well is located on the north side of the "PPG Area". Annular flow, at approximately 2 gpm was present. "PPG" plugging requirements will be necessary.
2118038441 2005-09-15 Final restoration is approved.
2155i90 2002-05-28 Met with Dan Cook (330-753-5081) with B & C Machine regarding the current status and future plans for this well. Mr. Cook indicated that the well does occasionally provide natural gas to the facility and is therefore in production. Advised Mr. Cook that the well lacked proper signage and spill containment around the tank battery. Also provided Mr. Cook with a copy of the Plugging Company list for future reference. Will check the site in several weeks to verify that the sign and dike were installed.
8779415 2002-05-23 Random status check. Operator has never reported production and according to facility employees, the well has not been in production for at least eight years. Well is equipped with one 210 bbl stock tank, one 60 bbl brine tank, one horizontal separator, and a pumping unit. Will call the operator re: any specific plans for the well.