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34-121-21803

Well Details

Well ID: 34-121-21803
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1975-11-24
Unconventional:
Horizontal:
Producing: No
Violations: 4
Latitude: 39.7426924301
Longitude: -81.6164996752

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-377341842 2004-08-27 Conversation with company rep John Schieder concerning plugging operation of said well,possible plug job9/1/04.Co.Rig ran 2mandrel in well to 4300' ran out of line moving Kilbarger in on Mon.
1087055863 2004-06-08 Stopped by service rig for update on possible plug/plugback of said well,Kilbarger Services of Logan contractor operator stated fluid level in well at 144' ran bare tools in well and sat down at 658' awaiting orders from company to continue with operation.
1094216022 2004-09-01 on site to witness setting of bottom hole plug,30sks cement plug@5225-4825 set through tubing.
1117300922 2005-05-23 On site to witness shooting off of casing casing was shoot off @3240',when rig crew hooked on casing it was parted@642' pulled pipe out awaiting orders from company office,company rep stated they would resume working on well 5/31/05 attempting to fish casing out of hole if unable to retrive pipe operator will finish plugging well,as of now operator is planning on producing Berea/Gordon sands if they can retrive pipe.
1118963143 2005-06-13 Stopped by service rig for update on completing plug-back operation,they were running 4.5 casing in well,ran2155' of new9.5 casing and cemented with 150 sk. Cement which should cover800' on backside of casing.
1340032303 2012-06-18 Inspection of the well head found the following equipment -4.5 production casing -2.375 tubing & rods with the well equipped with a pumping unit and the production valves open . A 100 barrel tank -separator and gas meter are present in an established dike with proper well identification present .
1467804548 2005-05-06 Service rig moved back in on site to finish plug-back operation,rig broke down awaiting parts to repair rig.
1706552017 2009-01-21 Well was plugged back to Berea/Ohio shale well is equipped with pumping unit and tubing&rods and 1-100 bbl with dike in place,no production has been reported on well since 2006.
1824967614 2004-01-15 FOLLOW UP TO NOV # 778040032 Upon inspecting well site found no I.D.posted at tank site or at wellhead no production chart found at site,no production reported on said well since 1997 well appears to be idle.Valves at wellhead are closed 4x2 swedge on 4.5casing. 9-9-05(A)10
1824967614 2004-01-15 FOLLOW UP TO NOV # 778040032 Upon inspecting well site found no I.D.posted at tank site or at wellhead no production chart found at site,no production reported on said well since 1997 well appears to be idle.Valves at wellhead are closed 4x2 swedge on 4.5casing. NONE
1979810147 2012-11-20 My inspection today finds the well is equipped with 4.5" casing, 2.375", tubing, rods, and a pump jack. The tank battery consists of one 100 bbl tank, a meter, and a separator. The tank is contained in a dike and has proper identification.
2004918088 2004-08-30 On site to witness running of tubing in hole for upcoming plugging operation.

Suspect possibe casing problem @648' ran 5225'of 1.5 tubing in well to enable operator to set bottom hole plug.

406914429 2005-06-01 Stopped by service rig for update on fishing job rig operator stated they had pipe on overshot did'nt know for sure if they retrieved pipe where they had shot off or not,what casing they had on trailer was in bad shape holes etc..They had originally shot it off@3230' when they got out of hole they had recovered 2730' of casing.will set rip plug later on in week operator stated they would set cement plug @2600-2400' and then log hole to determine what depth they would run casing in hole to produce berea/gordon sands.
778040032 2004-01-15 Upon inspecting well site found no I.D.posted at tank site or at wellhead no production chart found at site,no production reported on said well since 1997 well appears to be idle.Valves at wellhead are closed 4x2 swedge on 4.5casing. 9-9-05(A)10
778040032 2004-01-15 Upon inspecting well site found no I.D.posted at tank site or at wellhead no production chart found at site,no production reported on said well since 1997 well appears to be idle.Valves at wellhead are closed 4x2 swedge on 4.5casing. NONE
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