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34-103-23107

Well Details

Well ID: 34-103-23107
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1982-10-11
Unconventional:
Horizontal:
Producing: No
Violations: 2
Latitude: 41.1308327367
Longitude: -82.0649877095

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1451986228 2005-02-15 Well is equipped with pump jack, rods and tubing. Sun, 50 degrees.
-1525251805 2014-06-30 Inspected production well on 06/30/2014. The tank battery consists of 3-100 bbl steel tanks located within an earthen dike. The tank battery is used by multiple wells; identification is posted for many of the wells producing into it, but this well is not included. The well is equipped with a pump jack with an electric motor. A small amount of paraffin was noted in the area immediately around the wellhead that needs cleaned up. Well identification is clearly displayed at the wellhead as required. Jason Klauss with Harley Drilling was notified of these issues and will address them as soon as possible. No other problems were noted at the time of the inspection.
1113349660 2005-04-12 Called by Kirk of OEPA to investigate oil spill at a tank battery. Oil is pooling inside dike area. 4- 100 barrel tanks are in battery. Number 3 tank is seeping oil from under tank bottom. Met with Tim Harley and advised him of the violation. 9-9-05(A)1
1114170661 2005-04-21 Tanks were skidded and all oil soil was removed in and outside dike. Concrete vault has been pumped. Oil around well head removed. Electric lines buried. Violation in compliance. 9-9-05(A)1
PL11919 Preliminary Restoration done information from Data Point