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Well ID: 34-005-21791 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1976-08-27 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 5 | |
Latitude: 40.8959635406 | |
Longitude: -82.1558832874 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
-1082935222 | 2006-12-29 | NOV followup. Ran Mini test on annulus and pressure held at 410psi for 15 minutes. Injection pressure is at 350 psi. | ||||
-111963044 | 2007-03-30 | Injection and annulaus pressure test. Pressures are equalized at 350 psi. | 9-5-09[C] | |||
-1464663205 | 2013-05-08 | Operator pickled and cleaned casing with acid. Run tubing and packer with new rubbers and cage. Pressure test of well did not pass. Significant loss of pressure when tested. Five times a joint of pipe was pulled up, packer set, loaded with water and pressure tested. Each test failed. Tool pusher reported the packer would set down at a depth of 268 feet below grade. Pulled packer up and set at 257 ft. above obstruction. Pressure tested ok at 257. The following day the packer was set and tested at 293 ft., below obstruction. Pressure test failed. Hole in casing about 268 feet. Reviewed old records the original well was drilled 8 to 10 inches from current hole. Due to casing being pushed out of bore hole by shooting with nitroglycerin. Well will be plugged. | ||||
-1542833910 | 2008-12-11 | Injection and annulus pressure test. | ||||
-1565115727 | 2007-10-22 | Reset packer and tested but pressure equilized. Recommend pulling packer out and inspect. Shut well in until it will test. | ||||
-1565488129 | 2006-12-15 | Injection and annulus pressure test. Pressures are equalized at 350 psi. | 9-5-09[C] | |||
-1609952911 | 2012-02-27 | Inspect well. Valve on Annulus is broken. | ||||
-1722416447 | 2009-04-25 | Injection and annulus pressure test. | ||||
-1958963302 | 2007-04-03 | NOV in compliance. Blew down annulus and pressured up to 320 psi. Pressure held at 320 psi for 15 minutes. 0% decline. Injection pressure is 290 psi. Advised Matt Miller of injection pressure decline. Run mini test April 30, 2007 and report to inspector. | ||||
-208962727 | 2006-03-15 | Re-test annulus and tubing pressures. Nov in compliance. Snow, 29 degrees | 9-5-10(H) | |||
-279559499 | 2010-11-27 | Injection and annulus pressure test. | ||||
-43150819 | 2008-03-27 | Annulus and injection pressure test. | ||||
-473608655 | 2011-07-12 | inspect well | ||||
-502459913 | 2003-08-07 | UNABLE TO GAUGE INJECTION PRESSURE, NEED TO REPLACE WITH VALVE TAP FOR 1/4" OR 1/2" GAUGE | ||||
-503156724 | 2011-10-17 | Inspect well. | ||||
-511764643 | 2012-09-11 | Inspect Well. Site ok. | ||||
-625117970 | 2004-11-18 | Injection pressure test. | ||||
-735082993 | 2011-04-13 | Injection and annulus pressure test. | ||||
111057061 | 2010-04-06 | Injection and annulus pressure test. | ||||
1116355295 | 2005-05-17 | Injection well test. GPS location and update to RBDMS. | ||||
1192038614 | 2007-10-10 | Injection and annulus pressure test. Pressures are equalized at 330 psi. Suspended well operation at this time. | 9-5-09[C] | |||
1350741638 | 2012-06-04 | Inspect Well. Annulus valve was replaced. Box needs repair. | ||||
1371742425 | 2013-06-20 | Request from operator to witness well plugging. The well was plugged with 9 sack grout. | ||||
1376581904 | 2013-08-15 | The site needs to be graded and a pipe rack with 1 inch tubing removed to approve final restoration. Randy at Deep Resources was advised. He stated he would call when work is complete. | ||||
1850524506 | 2007-10-30 | Mechanical integrity test. Pulled 1 tubing and packer. Replaced packer and circulated inhibitor thru annulus and pressure tested packer and tubing at 350 psi. Drop of 10 psi in 15 minutes. NOV in compliance. Sun, 55 degrees. | ||||
1948417058 | 2004-04-22 | Injection pressure test. Could not test tubing pressure due to size of gauge threads. Advised Len Rex to install reducer and test. Report to Tom Tomastik in 30 days. | ||||
2018932901 | 2013-05-02 | Run packer and tubing into well, 21 joints at 25 feet each with a Butler Larkin 6 inch compression packer with new rubbers. Each individual joint of tubing was pressure tested for leaks. The packer was originally set at 525 feet. Formation gas was leaking past packer and the test was not successful. Operator will install tie downs to set and hold packer. | ||||
40325828 | 2012-12-04 | Inspect well for integrity and pressure. | ||||
510006879 | 2013-03-04 | Inspect well for integrity and pressure. | ||||
583280891 | 2005-12-01 | Injection and annulus pressure test. Pressures have equalized at 350 psi. | 9-5-10(H) | |||
751620049 | 2006-04-24 | Injection and annulus pressure test. | ||||
763086463 | 2013-04-04 | Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Test failed. Well shut in. | ||||
774942903 | 2013-10-17 | All equipment has been removed from the site. The location is finish graded and vegetated. Casing has been cut off. The final restoration is approved. | ||||
923400769 | 2009-10-07 | Injection and annulus pressure test. |