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Well ID: 34-119-27849 | Loading map...
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Operator Name: | |
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First Permit Date: | |
Last Permit Date: | |
Spud Date: 1994-02-15 | |
Unconventional: | |
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Producing: No | |
Violations: 0 | |
Latitude: 40.0976351014 | |
Longitude: -82.1323887188 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1684582801 | 2012-10-10 | Matheny well service is running 2.375tubing in to set Bottom plug at 5300-4900'. Formation Cementing spotted 30 sack plug. 18.9 barrel was the displacement with brine water. | ||||
-1784768670 | 2012-10-12 | On the day of my inspection Matheny Well Svc pulled 4353' of 11.6# 4.5" casing from the well, and Formation Cementing set 6 cement plugs at various intervals from 3880' to surface. See plug report for details. | ||||
-86998140 | 2012-10-10 | Matheny well service ripped 4.5casing at 4353' and pulled up to 3800' due to pulling tight. Formation Cementing set 100' rip plug. Formation set clinton plug at 3321'-3129. Chris Grimm witnessed rest of plug job. | ||||
1369242556 | 2013-05-22 | On day of inspection site has not vegetated back yet. I will look at later date. | ||||
1522861497 | 2008-07-21 | Producing, no problems noted. Pumping when I was there. | ||||
19084 | PASSED Y WITNESSED 11/18/94 INSPECTOR GERALD YOUNG DATE 11/1819/94 DATA FROM OLD VAX INFO |