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Well ID: 34-059-24190 | Loading map...
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County: | |
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Operator Name: | |
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First Permit Date: | |
Last Permit Date: | |
Spud Date: 2011-09-26 | |
Unconventional: | |
Horizontal: | |
Producing: | |
Violations: 0 | |
Latitude: 39.8720476441 | |
Longitude: -81.6838887428 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1025609309 | 2011-10-17 | Spud meeting at well site with rig crew and service personnel. | ||||
-1603889048 | 2011-11-21 | |||||
-1667347511 | 2011-11-21 | Total depth was reached at 10,962'. Will condition wellbore and then log well and possibly run casing later on in the week. | ||||
-1920651845 | 2012-02-22 | Stopped by drill site for update they were flowing well back into 500 bbl tanks and hauling water to UIC facility for proper disposal. | ||||
-2059153676 | 2011-10-12 | |||||
-596583758 | 2012-02-29 | Stopped by site for update they were still flowing well back to 500 bbl storage tanks and also were flaring gas through flare stack. | ||||
-748635310 | 2014-06-05 | On the day of my inspection the site passed preliminary restoration according to 1509.072A. | ||||
-892561045 | 2014-06-05 | On the day of my inspection the site passed preliminary restoration according to 1509.072A. | ||||
-95110996 | 2011-11-22 | Casing crew rigging up to run production casing. Owner is going to run split string of casing - 4.5" casing through lateral and 5.5" casing in vertical section. Top of cement will be brought up into the intermediate casing string. | ||||
1317069975 | 2011-09-26 | Zigenfuess Drilling on site to set conductor and intermediate pipe to 500' should be cementing 16" casing later on in week. | ||||
1317411697 | 2011-09-30 | Setting 24" casing@360' will possibly set 16" late tomorrow afternoon. | ||||
1319491047 | 2011-10-21 | On site to witness testing of BOP by Greene's Energy Group. Annular was tested at @ 3500 PSI and blind ram was tested at @ 5000 PSI. Pipe ram and choke system were also tested @ 5000 PSI. All equipment for BOP passed test. | ||||
33154408 | 2011-09-28 | Drilling 24" conductor hole they were@180' they propose to set 200'+- hopefully by tomorrow. |