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Well ID: 34-155-23381 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1991-01-25 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 0 | |
Latitude: 41.3025105023 | |
Longitude: -80.8000377003 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-682139156 | 2004-02-20 | Restoration approved . | ||||
102977810 | 2002-10-23 | Meets requirements. | ||||
1395241295 | 2014-03-19 | My inspection found the well in production. The well was equipped with a plunger lift unit. A domestic gas line came off the 4.5" casing. The tank battery consisted of a 100 barrel production tank, a 30 barrel brine tank, and a separator. The dike was slightly weathered; however, it meets containment requirements. An identification sign was staked into the berm of the dike. The information on the identification sign was highly faded. There was a bull plug on the load line. The lease road was in stable condition. The well was placed into production prior to House Bill 278. I called Dustin Energy and instructed the owner to fix the identification sign. Bill stated the information would be corrected immediately. |