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Well ID: 34-121-21978 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1977-08-18 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 2 | |
Latitude: 39.87134079 | |
Longitude: -81.4966093268 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1464532135 | 2013-04-12 | I am onsite to witness the placement of the bottom plug. A 30sk class A cement plug was placed at 5572' to 5179' through 2.375" tubing. | ||||
-1684566289 | 2013-04-11 | My inspection today finds the well is being plugged by Nicks Plugging. An attempt to pump through the tubing failed and the rig crew started to trip the 2.375" tunbing. | ||||
1366066194 | 2013-04-15 | Well has been plugged resolving previous notice issued on 2/3/12. | ||||
1420233896 | 2012-02-03 | Upon receiving request from landowner to inspect well site found well to be idle and last production reported on well was back in 2007,and well is equipped with 1-210 barrel tank with incomplete identification information and seperator with no chart in meter box and at wellhead there is 8.625" and 4.5" and 2.375" tubing and valves were closed on the day of my inspection,and after calling company rep stating that production casing has possible hole in it that is why well quit producing.
PLUG WELL OR REPAIR CASING AND PUT BACK INTO PRODUCTION. Failure to comply may result in bond forfieture. |
9-9-05(A)10 | |||
1420233896 | 2012-02-03 | Upon receiving request from landowner to inspect well site found well to be idle and last production reported on well was back in 2007,and well is equipped with 1-210 barrel tank with incomplete identification information and seperator with no chart in meter box and at wellhead there is 8.625" and 4.5" and 2.375" tubing and valves were closed on the day of my inspection,and after calling company rep stating that production casing has possible hole in it that is why well quit producing.
PLUG WELL OR REPAIR CASING AND PUT BACK INTO PRODUCTION. Failure to comply may result in bond forfieture. |
NONE | |||
855137577 | 2012-02-03 | FOLLOW UP TO NOV # 1420233896 Upon receiving request from landowner to inspect well site found well to be idle and last production reported on well was back in 2007,and well is equipped with 1-210 barrel tank with incomplete identification information and seperator with no chart in meter box and at wellhead there is 8.625" and 4.5" and 2.375" tubing and valves were closed on the day of my inspection,and after calling company rep stating that production casing has possible hole in it that is why well quit producing.
PLUG WELL OR REPAIR CASING AND PUT BACK INTO PRODUCTION. Failure to comply may result in bond forfieture. |